QFR No - 8000859512
Defect Details
NC No. 8000859512
NC Date 19/01/2024
NC Submission Date
Part No. 520KT00102
Part Name ROD BUSH
Supplier Name & Code 100176-GKN SINTER METALS PRIVATE LIMI
ETL Plant 1146-ETL Suspension Narasapura
Defect Details MATERIAL DEFECT-CRACK ISSUE
 
1. Problem Description
Defect Description Rod bush crack issue
Detection Stage Inprocess
Problem Severity Safety
NG Quantity 272
Is Defect Repeatative? No
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID Rajendra.Sethiya@gknpm.com
Plant Head/CEO Email ID Pratik.Dharangaonkar@gknpm.com
MD Email ID Rajesh.Mirani@gknpm.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
46000
0
0
23000
0
69000
Check Qty
46000
0
0
23000
0
69000
NG Qty
274
0
0
0
0
274
 
Scrap 274
Rework 0
Under Deviation 0
Containment Action
Stock lying at ETL end & GKN end segregated for crack issue.
 
3. Process Flow
Process Flow Description
Mixing-Forming-Sintering-Heat Treatment-Barreling-Final Inspection-PDI
 
4. Process Details
Process / Operation Forming
Outsource No
Machine / Cell Forming Press
Machine / Cell No. NA
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MethodForming material handling inadequateMaterial is handled in plywood trays at forming stageX
ManUnskilled OperatorSkill matrix verified, found OKO
ToolWrong tools usedTools report verified, found OKO
MaterialRaw material NGRM Test report verified, found OKO
MaterialDensity NGMTR Verified, found OKO
MaterialHardness NGMTR Verified, found OKO
MachineMachine breakdownIn process reports verified, found OKO
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method Visual Inspection
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100 %
7. Root Cause Analysis (Occurance)
Why 1 Crack observed in rod bush
Why 2 Crack got generated during handling of material at sintering stage
Why 3 During forming to sintering material handled plywood trays
Why 4 During sintering material loaded in wire mesh trays from plywood trays
Why 5
Root Cause (Occurance) During sintering material loaded in wire mesh trays from plywood trays
 
Root Cause Analysis (Outflow)
Why 1 Crack observed in rod bush
Why 2 Crack part skipped from visual inspection
Why 3 No check point available at final inspection
Why 4
Why 5
Root Cause (Outflow) No check point available at final inspection
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceAwareness training given to concern operators to use wire mesh trays instead of plywood traysMr. Rohan G15/04/202413/04/2024Completed
OutflowCheckpoint added at final inspection WIMr. B Avhad15/04/202413/04/2024Completed
OccuranceFrom forming to sintering material will be handled in wire mesh trays instead of plywood traysMr. Rohan G15/04/202413/04/2024Completed
OutflowAwareness training given to concern personsMr. B Avhad15/04/202413/04/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System No
Change Details NA
Inspection Method Other
Other Inspection Method Visual Inspection
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100 %
10. Evidance of Countermeasure
Occurance (Before) Plywood trays used
642_Occurance_Before.pptx
Occurance (After) Wire mesh trays implemented
642_Occurance_After.pptx
Outflow (Before) No check point
642_Outflow_Before.ppt
Outflow (After) Check point added
642_Outflow_After.ppt
 
11. Horizontal Deployment
Horizontal Deployment Required No
Applicable Machine / Model / Plant NA
 
12. Document Review
Documents ControlPlan, PFMEA, WISOP
Specify Other Document NA
 
13. Effectiveness Of Action
Reviewed Quantity 1000
Reason for submission problem in rod bush but in action plan photo piston