QFR No - 8000862973
Defect Details
NC No. 8000862973
NC Date 14/02/2024
NC Submission Date
Part No. F2LY02502B
Part Name SOCKET HEADED BOLT - RE J1A
Supplier Name & Code 100846-SANGKAJ ENGINEERING PVT.LTD.
ETL Plant 1117-ETL K-228/9 Suspension
Defect Details NOT AS PER SPECIFICATION-PLATING THICKNESS FOUND NOT OK
 
1. Problem Description
Defect Description Pinch bolt - J1C plating thickness found 6 to 8 microns against 8 microns minimum
Detection Stage Customer End
Problem Severity Aesthetic
NG Quantity 6200
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID sepl.quality@sangkaj.com
Plant Head/CEO Email ID steel@sangkaj.com
MD Email ID anirudh.2007@hotmail.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
6200
0
0
0
0
6200
Check Qty
6200
0
0
0
0
6200
NG Qty
6200
0
0
0
0
6200
 
Scrap 0
Rework 6200
Under Deviation 0
Containment Action
rework done on all part
 
3. Process Flow
Process Flow Description
Wire Draw - Cold Forging - Thread Rolling - HT - Plating - F.I. - Dispatch.
 
4. Process Details
Process / Operation Plating
Outsource Yes
Machine / Cell Plating
Machine / Cell No. Auto Line
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MethodDue to excess loading in a batch qtyCause VerfiedO
 
6. Inspection Method Analysis (Current)
Inspection Method Instrument
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 10 Nos
7. Root Cause Analysis (Occurance)
Why 1 Thickness at lower side
Why 2 Current fluctuation observed
Why 3 Current not properly distributed
Why 4 Due to excess loading in a batch qty ( 50 Kg against 40 Kg )
Why 5 Manually batch quantity taken on weighting scale
Root Cause (Occurance) Manually batch quantity taken on weighting scale
 
Root Cause Analysis (Outflow)
Why 1 Plating Thickness at lower side
Why 2 Not detected at final inspection.
Why 3 Measurement variation observed.
Why 4 in DFT meter plating thickness not get proper reading.
Why 5
Root Cause (Outflow) in DFT meter plating thickness not get proper reading.
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceOnline weighting interlock system implementationKrishna Industries15/03/202407/03/2024Completed
OutflowNow every batchwise samples is getting checked by XRF .Krishna Industries16/02/202416/02/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details Now every batch-wise samples is getting checked by XRF
Inspection Method Instrument
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 30 Nos
10. Evidance of Countermeasure
Occurance (Before) Manualy batch quantity taken on weighting scale
679_Occurance_Before.pptx
Occurance (After) We are implementing the online weighting interlock system with over load alarm /buzzer
679_Occurance_After.pptx
Outflow (Before) We checked batch wise thickness on in house thickness tester
679_Outflow_Before.xlsx
Outflow (After) Now every batch wise samples is getting checked by XRF.
679_Outflow_After.pdf
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant All Plated Parts.
 
12. Document Review
Documents ControlPlan, PokayokeCheckSheet
Specify Other Document No
 
13. Effectiveness Of Action
Reviewed Quantity 567
Reason for submission Found ok