QFR No - 8000862973
Defect Details
NC No. | 8000862973 |
NC Date | 14/02/2024 |
NC Submission Date | |
Part No. | F2LY02502B |
Part Name | SOCKET HEADED BOLT - RE J1A |
Supplier Name & Code | 100846-SANGKAJ ENGINEERING PVT.LTD. |
ETL Plant | 1117-ETL K-228/9 Suspension |
Defect Details | NOT AS PER SPECIFICATION-PLATING THICKNESS FOUND NOT OK |
1. Problem Description
Defect Description | Pinch bolt - J1C plating thickness found 6 to 8 microns against 8 microns minimum |
Detection Stage | Customer End |
Problem Severity | Aesthetic |
NG Quantity | 6200 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | sepl.quality@sangkaj.com |
Plant Head/CEO Email ID | steel@sangkaj.com |
MD Email ID | anirudh.2007@hotmail.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
6200
|
0
|
0
|
0
|
0
|
6200
|
Check Qty |
6200
|
0
|
0
|
0
|
0
|
6200
|
NG Qty |
6200
|
0
|
0
|
0
|
0
|
6200
|
Scrap | 0 |
Rework | 6200 |
Under Deviation | 0 |
Containment Action |
---|
rework done on all part |
3. Process Flow
Process Flow Description |
---|
Wire Draw - Cold Forging - Thread Rolling - HT - Plating - F.I. - Dispatch. |
4. Process Details
Process / Operation | Plating |
Outsource | Yes |
Machine / Cell | Plating |
Machine / Cell No. | Auto Line |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Method | Due to excess loading in a batch qty | Cause Verfied | O |
6. Inspection Method Analysis (Current)
Inspection Method | Instrument |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 10 Nos |
7. Root Cause Analysis (Occurance)
Why 1 | Thickness at lower side |
Why 2 | Current fluctuation observed |
Why 3 | Current not properly distributed |
Why 4 | Due to excess loading in a batch qty ( 50 Kg against 40 Kg ) |
Why 5 | Manually batch quantity taken on weighting scale |
Root Cause (Occurance) | Manually batch quantity taken on weighting scale |
Root Cause Analysis (Outflow)
Why 1 | Plating Thickness at lower side |
Why 2 | Not detected at final inspection. |
Why 3 | Measurement variation observed. |
Why 4 | in DFT meter plating thickness not get proper reading. |
Why 5 | |
Root Cause (Outflow) | in DFT meter plating thickness not get proper reading. |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | Online weighting interlock system implementation | Krishna Industries | 15/03/2024 | 07/03/2024 | Completed |
Outflow | Now every batchwise samples is getting checked by XRF . | Krishna Industries | 16/02/2024 | 16/02/2024 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | Now every batch-wise samples is getting checked by XRF |
Inspection Method | Instrument |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 30 Nos |
10. Evidance of Countermeasure
Occurance (Before) |
Manualy batch quantity taken on weighting scale 679_Occurance_Before.pptx |
Occurance (After) |
We are implementing the online weighting interlock system with over load alarm /buzzer 679_Occurance_After.pptx |
Outflow (Before) |
We checked batch wise thickness on in house thickness tester 679_Outflow_Before.xlsx |
Outflow (After) |
Now every batch wise samples is getting checked by XRF. 679_Outflow_After.pdf |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | All Plated Parts. |
12. Document Review
Documents | ControlPlan, PokayokeCheckSheet |
Specify Other Document | No |
13. Effectiveness Of Action
Reviewed Quantity | 567 |
Reason for submission | Found ok |