QFR No - 8000873489
Defect Details
NC No. 8000873489
NC Date 06/05/2024
NC Submission Date
Part No. F2LG05302B
Part Name SEAT PIPE - ABWB ENDURO
Supplier Name & Code 100929-HARSHAD ENGINEERING COMPANY
ETL Plant 1117-ETL K-228/9 Suspension
Defect Details NOT AS PER SPECIFICATION-THREAD MISSING
 
1. Problem Description
Defect Description THREAD MISSING
Detection Stage Inprocess
Problem Severity Fitment
NG Quantity 1
Is Defect Repeatative? No
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID qaharshad@miteshauto.com
Plant Head/CEO Email ID sjkadam@miteshauto.com
MD Email ID auto.mitesh@gmail.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
500
200
0
0
0
700
Check Qty
500
200
0
0
0
700
NG Qty
1
0
0
0
0
1
 
Scrap 1
Rework 0
Under Deviation 0
Containment Action
100 % sorting done for ETL End, HEC WIP & FG material
 
3. Process Flow
Process Flow Description
Cutting-Draw-Forging(Head Formation)-Rough Grinding-CNC (Head, Boring & Tapping)-Punching-Finish Grinding-Final Inspection-Packing-Dispatch
 
4. Process Details
Process / Operation Tapping
Outsource No
Machine / Cell Tapping
Machine / Cell No. 164
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MethodSkip While Visual InspectionSkip While InspectionX
MachineLimit Switch setting not ok or Malfunction while workingLimit switch malfunction while workingX
ToolTap Worn out or damageTap found in OK ConditionO
ManInspection or Checking SkippedAs per Sampling plan parts checked by InspectorsO
MaterialWrong grade material UsedMaterial grade is ok As per DrawingO
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method Visually
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
7. Root Cause Analysis (Occurance)
Why 1 Threading missing
Why 2 During tapping operation tap not performed threading
Why 3 Threading spindle limit switch not working properly
Why 4 Threading limit switch mal-function
Why 5
Root Cause (Occurance) Threading limit switch mal-function
 
Root Cause Analysis (Outflow)
Why 1 Threading missing
Why 2 100% parts not checked at final inspection stage
Why 3 Parts checked on sampling basis
Why 4
Why 5
Root Cause (Outflow) Parts checked on sampling basis
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceIn PM check sheet point added for Limit switch checkingMMS15/05/202417/05/2024Completed
OccuranceLimit switch changed with new oneProduction team10/05/202412/05/2024Completed
Outflow100% parts visually checked at final inspectionQA Team03/05/202408/05/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details 100% parts checked at final inspection stage with identification
Inspection Method Other
Other Inspection Method Visually
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) Limit switch mal function
782_Occurance_Before.pdf
Occurance (After) Limit switch changed and in PM check sheet point added
782_Occurance_After.pdf
Outflow (Before) Parts Checked on sampling basis
782_Outflow_Before.jpg
Outflow (After) 100% Parts Checked for threading presence
782_Outflow_After.jpg
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant For all model of seat pipe
 
12. Document Review
Documents ControlPlan, WISOP
Specify Other Document CP, PM checksheet
 
13. Effectiveness Of Action
Reviewed Quantity 100
Reason for submission ok