QFR No - 8000874016
Defect Details
NC No. 8000874016
NC Date 11/05/2024
NC Submission Date
Part No. F20510907B
Part Name UNDER BRACKET ASSEMBLY K19 DRUM FF
Supplier Name & Code 100297-BAJAJSONS LTD
ETL Plant 1126-ETL Pantnagar
Defect Details THREADING NOT OK-THREAD LENGTH UNDERSIZE
 
1. Problem Description
Defect Description Thread Length Undersize observed 10.50 to 11.20 against the specs. 12+1.0
Detection Stage Inprocess
Problem Severity Fitment
NG Quantity 4
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID anuj.saxena@bajajsons.com
Plant Head/CEO Email ID sahadev.singh@bajajsons.com
MD Email ID sanjay.bajaj@bajajsons.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
1500
0
0
400
2250
4150
Check Qty
1500
0
0
400
2250
4150
NG Qty
4
0
0
0
0
4
 
Scrap 4
Rework 0
Under Deviation 0
Containment Action
All material has been segregated at ETL end as well as Bajajsons Roorkee end.
 
3. Process Flow
Process Flow Description
1-Parting 2-Flaring & Reducing 3-Bush Fitting 4-Bush welding 5-CNC turning 6-Grinding 7-Threading 8-To Assembly
 
4. Process Details
Process / Operation Threading
Outsource No
Machine / Cell TDR-11/Shaft Line
Machine / Cell No. TDR-11
5. Problem Analysis
Type Possible Cause Fact Verification Jud
ManUnskilled operator.Unskilled operatorX
MachinePart not proper butting with stopper.Dust particles stick to stopper face at TDRX
 
6. Inspection Method Analysis (Current)
Inspection Method Instrument
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
7. Root Cause Analysis (Occurance)
Why 1 Threading process was NG
Why 2 Proper part feeding was not ok
Why 3 Part does not rest at stopper face
Why 4 Dust particles stick to stopper face at TDR
Why 5
Root Cause (Occurance) Dust particles stick to stopper face at TDR
 
Root Cause Analysis (Outflow)
Why 1 Thread length u/s
Why 2 Only sampling inspection being done at final inspection for thread length checking inspection.
Why 3
Why 4
Why 5
Root Cause (Outflow) 100% Inspection not done at final inspection.
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OutflowOPL has been displayed at final inspection. 100% inspection started at FI to check thread length by visually.Mr. Vikash23/05/202422/05/2024Completed
OccuranceTraining has been given to operator that feeding the part after remove the dust particles at stopperMr. Mukesh chauchan25/05/202422/05/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details 100% Visually inspection started
Inspection Method Other
Other Inspection Method Visually
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) Stopper Pic & On Job Training
797_Occurance_Before.jpg
Occurance (After) Stopper Pic & On job Training
797_Occurance_After.jpg
Outflow (Before) No OPL displayed
797_Outflow_Before.pdf
Outflow (After) OPL
797_Outflow_After.pdf
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant B104D/B105L
 
12. Document Review
Documents ControlPlan
Specify Other Document OPL
 
13. Effectiveness Of Action
Reviewed Quantity 1
Reason for submission OK