QFR No - 8000876572
Defect Details
NC No. 8000876572
NC Date 30/05/2024
NC Submission Date
Part No. 165FG01001
Part Name GEAR PRIMARY ASSY 3W-4S 200CC MAX CNG
Supplier Name & Code 100237-SANJEEV AUTO PARTS MRFS PVT LT
ETL Plant 1132-ETL K-226/1 TRANSMISSION
Defect Details MIX UP OTHER MODEL-WRONG HOBBING ISSUE (74 TEETH)
 
1. Problem Description
Defect Description Wrong teeth Hobbing done (74 teeth Hobbing done instead of 77 Nos)
Detection Stage Inprocess
Problem Severity Fitment
NG Quantity 1
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID vpwankhade@sanjeevgroup.com
Plant Head/CEO Email ID rmtiwari@sanjeevgroup.com
MD Email ID maithilee@sanjeevgroup.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
350
0
0
200
200
750
Check Qty
350
0
0
200
200
750
NG Qty
0
0
0
0
0
0
 
Scrap 0
Rework 0
Under Deviation 0
Containment Action
100% material checked at WIP & final inspection, Confirmed with tick mark iderntifiction to ensure defect free parts.
 
3. Process Flow
Process Flow Description
Raw Material Inward Bar Cutting Billet Heating Hot Forging Normalizing Shotblasting Coining Preturning Peircing-1 Peircing-2 Shaving-1 Shaving-2 Milling-1 Milling-2 Finish turning 1st setup Finish turning 2nd setup Finish turning 3rd setup Deburring Final Inspection CNC Blank Inward Inspection CNC Blank Traciability Marking Hobbing Teeth Chamfering Gear Shaving Heat tratment Shotblasting ID Turning Bush Pressing Bush Turning Washing Final inspection
 
4. Process Details
Process / Operation Hobbing
Outsource No
Machine / Cell GPH Cell
Machine / Cell No. Gleason -1
5. Problem Analysis
-------
Type Possible Cause Fact Verification Jud
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method Visual
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
7. Root Cause Analysis (Occurance)
Why 1 MIX UP OTHER MODEL-WRONG HOBBING ISSUE (74 TEETH)
Why 2 WRONG CNC BLANKLOADED FOR HOBBING
Why 3 VERIFICATION OF BLANK NOT DONE BEFORE LOADING FOR HOBBING
Why 4 VERIFICATION (INPECTION) SKIPPED
Why 5
Root Cause (Occurance) VERIFICATION (INPECTION) SKIPPED
 
Root Cause Analysis (Outflow)
Why 1 MIX UP OTHER MODEL-WRONG HOBBING ISSUE (74 TEETH)
Why 2 NOT ARRESTED DURING DFCE INSPECTION
Why 3 DIAL PRESSURE SCALE VALUE INSPECTION SKIPPED DURING DFCE INSPECTION
Why 4
Why 5
Root Cause (Outflow) DIAL PRESSURE SCALE VALUE INSPECTION SKIPPED DURING DFCE INSPECTION
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceOPL DISPLAYED AT HOBBINGVGW04/06/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details CONFIRMATION MARKING FOR DIAL PRESSURE SCALE VALUE DURING DFCE INSPECTION
Inspection Method Other
Other Inspection Method GEAR ROLLING TESTER
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) WRONG PART LOADED DURING HOBBING VERIFICATION SKIPPED
832_Occurance_Before.pptx
Occurance (After) Q ALERT DISPLAYED AT HOBBING FOR IDENTIFICATION OF CNC PART
832_Occurance_After.pdf
Outflow (Before) DIAL PRESSURE SCALE VALUE INSPECTION SKIPPED DURING DFCE INSPECTION
832_Outflow_Before.pptx
Outflow (After) Q ALERT DISPLAYED AT FINAL INSPECTION FOR INSPECTION OF DIAL PRESSURE SCALE VALUE
832_Outflow_After.pdf
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant ALL MODEL GPH
 
12. Document Review
Documents AuditCheckSheet
Specify Other Document Inprocess audit
 
13. Effectiveness Of Action
Reviewed Quantity
Reason for submission