QFR No - 8000877870
Defect Details
NC No. 8000877870
NC Date 11/06/2024
NC Submission Date
Part No. F2PH00902B
Part Name VALVE RETAINER (C101B)
Supplier Name & Code 101255-MAHAVIR INDUSTRIES
ETL Plant 1117-ETL K-228/9 Suspension
Defect Details NOT AS PER SPECIFICATION-CUT MAK
 
1. Problem Description
Defect Description CUT MAK
Detection Stage Inprocess
Problem Severity Fitment
NG Quantity 6
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID quality@mahavirind.co.in
Plant Head/CEO Email ID planthead@mahavirind.co.in
MD Email ID
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
3285
0
0
0
6000
9285
Check Qty
3285
0
0
0
6000
9285
NG Qty
6
0
0
0
0
6
 
Scrap 6
Rework 0
Under Deviation 0
Containment Action
All Suspected Material Segregation at Customer End
 
3. Process Flow
Process Flow Description
RM Inward - Store- Parting on Traub Machine - CNC counter boring and facing - OD Grinding- plating-- Final Inspection - Dispatch
 
4. Process Details
Process / Operation OD Grinding
Outsource No
Machine / Cell Grinding machine
Machine / Cell No. GRD-5
5. Problem Analysis
Type Possible Cause Fact Verification Jud
ManUnskilled operatorAs per Skilled Matrix Operator is SkilledO
MethodProcess &Inspection Method WrongProcess Method Ok But Inspection Method After OD Grinding visual frequency Very Low .X
MaterialHard And other grade Material UseHardness 75-80 HRB and as per required grade CEW-1 Material Use.O
ToolWrong Grinding Wheel UseAs Per Store Record Ok CUMI Make Grinding Wheel Use.O
MachineMachine Condition Not oK or RPM overMachine Condition ok But Control Wheel RPM was 45-60X
 
6. Inspection Method Analysis (Current)
Inspection Method Sp. Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 20/500nos
7. Root Cause Analysis (Occurance)
Why 1 NOT AS PER SPECIFICATION-CUT MAK
Why 2 Part Not Proper OD Grinding On Grinding Machine
Why 3 While OD grinding process, the part gets inverted.
Why 4 Control Wheel RPM was Over
Why 5
Root Cause (Occurance) Control Wheel RPM was Over
 
Root Cause Analysis (Outflow)
Why 1 NOT AS PER SPECIFICATION-CUT MAK
Why 2 Final Inspection stage Not Detect During Visual sampling Inspection ..
Why 3 After OD Grinding Process & Final Inspection stage visual frequency Very Low .
Why 4
Why 5
Root Cause (Outflow) After OD Grinding Process & Final Inspection stage visual frequency Very Low .
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceControl wheel RPM Reduce 30-45 Instead Of 45-60Production Head15/06/202415/06/2024Completed
OutflowSampling Frequency Increase 50nos Per 500Nos Instead Of 20/500nos& After Visual Inspection Tick Marks On OD at Final Stage.Quality Head17/06/202415/06/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details Sampling Frequency Increase & After Visual Inspection Tick Marks On OD at Final Stage.
Inspection Method Other
Other Inspection Method Visual
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 50Nos/500N
10. Evidance of Countermeasure
Occurance (Before) Control Wheel RPM was Over
856_Occurance_Before.docx
Occurance (After) Control wheel RPM Reduce 30-45 Instead Of 45-60
856_Occurance_After.docx
Outflow (Before) After OD Grinding Process & Final Inspection stage visual frequency Very Low .
856_Outflow_Before.docx
Outflow (After) Sampling Frequency Increase 50nos Per 500Nos Instead Of 20/500nos& After Visual Inspection Tick Marks On OD at Final Stage.
856_Outflow_After.docx
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant All CAP OIL Models
 
12. Document Review
Documents ControlPlan, PFMEA
Specify Other Document No
 
13. Effectiveness Of Action
Reviewed Quantity 150
Reason for submission OK