QFR No - 8000877870
Defect Details
NC No. | 8000877870 |
NC Date | 11/06/2024 |
NC Submission Date | |
Part No. | F2PH00902B |
Part Name | VALVE RETAINER (C101B) |
Supplier Name & Code | 101255-MAHAVIR INDUSTRIES |
ETL Plant | 1117-ETL K-228/9 Suspension |
Defect Details | NOT AS PER SPECIFICATION-CUT MAK |
1. Problem Description
Defect Description | CUT MAK |
Detection Stage | Inprocess |
Problem Severity | Fitment |
NG Quantity | 6 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | quality@mahavirind.co.in |
Plant Head/CEO Email ID | planthead@mahavirind.co.in |
MD Email ID |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
3285
|
0
|
0
|
0
|
6000
|
9285
|
Check Qty |
3285
|
0
|
0
|
0
|
6000
|
9285
|
NG Qty |
6
|
0
|
0
|
0
|
0
|
6
|
Scrap | 6 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
All Suspected Material Segregation at Customer End |
3. Process Flow
Process Flow Description |
---|
RM Inward - Store- Parting on Traub Machine - CNC counter boring and facing - OD Grinding- plating-- Final Inspection - Dispatch |
4. Process Details
Process / Operation | OD Grinding |
Outsource | No |
Machine / Cell | Grinding machine |
Machine / Cell No. | GRD-5 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Man | Unskilled operator | As per Skilled Matrix Operator is Skilled | O |
Method | Process &Inspection Method Wrong | Process Method Ok But Inspection Method After OD Grinding visual frequency Very Low . | X |
Material | Hard And other grade Material Use | Hardness 75-80 HRB and as per required grade CEW-1 Material Use. | O |
Tool | Wrong Grinding Wheel Use | As Per Store Record Ok CUMI Make Grinding Wheel Use. | O |
Machine | Machine Condition Not oK or RPM over | Machine Condition ok But Control Wheel RPM was 45-60 | X |
6. Inspection Method Analysis (Current)
Inspection Method | Sp. Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 20/500nos |
7. Root Cause Analysis (Occurance)
Why 1 | NOT AS PER SPECIFICATION-CUT MAK |
Why 2 | Part Not Proper OD Grinding On Grinding Machine |
Why 3 | While OD grinding process, the part gets inverted. |
Why 4 | Control Wheel RPM was Over |
Why 5 | |
Root Cause (Occurance) | Control Wheel RPM was Over |
Root Cause Analysis (Outflow)
Why 1 | NOT AS PER SPECIFICATION-CUT MAK |
Why 2 | Final Inspection stage Not Detect During Visual sampling Inspection .. |
Why 3 | After OD Grinding Process & Final Inspection stage visual frequency Very Low . |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | After OD Grinding Process & Final Inspection stage visual frequency Very Low . |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | Control wheel RPM Reduce 30-45 Instead Of 45-60 | Production Head | 15/06/2024 | 15/06/2024 | Completed |
Outflow | Sampling Frequency Increase 50nos Per 500Nos Instead Of 20/500nos& After Visual Inspection Tick Marks On OD at Final Stage. | Quality Head | 17/06/2024 | 15/06/2024 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | Sampling Frequency Increase & After Visual Inspection Tick Marks On OD at Final Stage. |
Inspection Method | Other |
Other Inspection Method | Visual |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 50Nos/500N |
10. Evidance of Countermeasure
Occurance (Before) |
Control Wheel RPM was Over 856_Occurance_Before.docx |
Occurance (After) |
Control wheel RPM Reduce 30-45 Instead Of 45-60 856_Occurance_After.docx |
Outflow (Before) |
After OD Grinding Process & Final Inspection stage visual frequency Very Low . 856_Outflow_Before.docx |
Outflow (After) |
Sampling Frequency Increase 50nos Per 500Nos Instead Of 20/500nos& After Visual Inspection Tick Marks On OD at Final Stage. 856_Outflow_After.docx |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | All CAP OIL Models |
12. Document Review
Documents | ControlPlan, PFMEA |
Specify Other Document | No |
13. Effectiveness Of Action
Reviewed Quantity | 150 |
Reason for submission | OK |