QFR No - 8000877871
Defect Details
NC No. | 8000877871 |
NC Date | 11/06/2024 |
NC Submission Date | |
Part No. | 520HL00202 |
Part Name | OIL LOCK COLLAR |
Supplier Name & Code | 100176-GKN SINTER METALS PRIVATE LIMI |
ETL Plant | 1117-ETL K-228/9 Suspension |
Defect Details | NOT AS PER SPECIFICATION-CRACK - MATERIAL DEFECT |
1. Problem Description
Defect Description | CUT MAK |
Detection Stage | Inprocess |
Problem Severity | Fitment |
NG Quantity | 5 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | nitin.palve@gknpm.com |
Plant Head/CEO Email ID | Deepak.jadhav@gknpm.com |
MD Email ID | Rajesh.Mirani@gknpm.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
14000
|
28000
|
0
|
0
|
0
|
42000
|
Check Qty |
14000
|
28000
|
0
|
0
|
0
|
42000
|
NG Qty |
7000
|
12
|
0
|
0
|
0
|
7012
|
Scrap | 7000 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
Quality Alert raised at In process area. Awareness training given to all concern stakeholders. All stock is under |
3. Process Flow
Process Flow Description |
---|
Mixing-Forming-Sintering- Barreling- Steam treatment PDI |
4. Process Details
Process / Operation | Forming |
Outsource | No |
Machine / Cell | Smal segment |
Machine / Cell No. | Plant 1 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Man | New Operator | Operator Skill Matrix verified | O |
Method | Parts fallen in rotary table due to conveyer height mismatch | Past history of concerned batch verified & Observed Excess gap creating impact on OD | X |
Material | Wrong Mix | MTR | O |
6. Inspection Method Analysis (Current)
Inspection Method | Other |
Other Inspection Method | Sampling Inspection |
Check Point at Final Inspection | No |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 5 |
7. Root Cause Analysis (Occurance)
Why 1 | Crack Generated on OD During Forming Process |
Why 2 | Impact generated on part OD on Rotary table during transferring from conveyor |
Why 3 | Excess gap between Rotary table & Conveyor Chute end |
Why 4 | No Checkpoint to verify gap |
Why 5 | |
Root Cause (Occurance) | Excess gap between Rotary table & Conveyor Chute end resulted into excess impact on part OD |
Root Cause Analysis (Outflow)
Why 1 | Crack Parts outflown to ETL |
Why 2 | Crack parts not detected during Inspection |
Why 3 | Inspection Frequency not adequate |
Why 4 | Inspection done on sampling basis |
Why 5 | |
Root Cause (Outflow) | Inspection done on sampling basis |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Outflow | Inspection Frequency Revised from 5 Parts / 4 Hours to 5 Parts/1 Hour | Rohan G | 04/07/2024 | 22/07/2024 | Completed |
Occurance | Glide Path Provided between Rotary table & Conveyer Clearence to avoid Impact | Rohan Gunwant | 04/07/2024 | 22/07/2024 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | Inspection frequency Revised from 5/8 Hour to 5 Parts/1 hour |
Inspection Method | Other |
Other Inspection Method | Visual Inspection |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 10 Nos |
10. Evidance of Countermeasure
Occurance (Before) |
Excess Gap on Rotary Table 857_Occurance_Before.pptx |
Occurance (After) |
Gap Eliminated to avoid stuck up issue 857_Occurance_After.pptx |
Outflow (Before) |
Before Inspection Frequency 5 Parts/8 Hour 857_Outflow_Before.pdf |
Outflow (After) |
After Inspection Frequency 5 Parts/ 1 Hour 857_Outflow_After.pdf |
11. Horizontal Deployment
Horizontal Deployment Required | No |
Applicable Machine / Model / Plant | NA |
12. Document Review
Documents | ControlPlan, PFMEA |
Specify Other Document | NA |
13. Effectiveness Of Action
Reviewed Quantity | 100 |
Reason for submission | OK |