QFR No - 8000877871
Defect Details
NC No. 8000877871
NC Date 11/06/2024
NC Submission Date
Part No. 520HL00202
Part Name OIL LOCK COLLAR
Supplier Name & Code 100176-GKN SINTER METALS PRIVATE LIMI
ETL Plant 1117-ETL K-228/9 Suspension
Defect Details NOT AS PER SPECIFICATION-CRACK - MATERIAL DEFECT
 
1. Problem Description
Defect Description CUT MAK
Detection Stage Inprocess
Problem Severity Fitment
NG Quantity 5
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID nitin.palve@gknpm.com
Plant Head/CEO Email ID Deepak.jadhav@gknpm.com
MD Email ID Rajesh.Mirani@gknpm.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
14000
28000
0
0
0
42000
Check Qty
14000
28000
0
0
0
42000
NG Qty
7000
12
0
0
0
7012
 
Scrap 7000
Rework 0
Under Deviation 0
Containment Action
Quality Alert raised at In process area. Awareness training given to all concern stakeholders. All stock is under
 
3. Process Flow
Process Flow Description
Mixing-Forming-Sintering- Barreling- Steam treatment PDI
 
4. Process Details
Process / Operation Forming
Outsource No
Machine / Cell Smal segment
Machine / Cell No. Plant 1
5. Problem Analysis
Type Possible Cause Fact Verification Jud
ManNew OperatorOperator Skill Matrix verifiedO
MethodParts fallen in rotary table due to conveyer height mismatchPast history of concerned batch verified & Observed Excess gap creating impact on ODX
MaterialWrong MixMTRO
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method Sampling Inspection
Check Point at Final Inspection No
Checking Freq. Sampling
Sampling No
Sample Size 5
7. Root Cause Analysis (Occurance)
Why 1 Crack Generated on OD During Forming Process
Why 2 Impact generated on part OD on Rotary table during transferring from conveyor
Why 3 Excess gap between Rotary table & Conveyor Chute end
Why 4 No Checkpoint to verify gap
Why 5
Root Cause (Occurance) Excess gap between Rotary table & Conveyor Chute end resulted into excess impact on part OD
 
Root Cause Analysis (Outflow)
Why 1 Crack Parts outflown to ETL
Why 2 Crack parts not detected during Inspection
Why 3 Inspection Frequency not adequate
Why 4 Inspection done on sampling basis
Why 5
Root Cause (Outflow) Inspection done on sampling basis
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OutflowInspection Frequency Revised from 5 Parts / 4 Hours to 5 Parts/1 HourRohan G04/07/202422/07/2024Completed
OccuranceGlide Path Provided between Rotary table & Conveyer Clearence to avoid ImpactRohan Gunwant04/07/202422/07/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details Inspection frequency Revised from 5/8 Hour to 5 Parts/1 hour
Inspection Method Other
Other Inspection Method Visual Inspection
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 10 Nos
10. Evidance of Countermeasure
Occurance (Before) Excess Gap on Rotary Table
857_Occurance_Before.pptx
Occurance (After) Gap Eliminated to avoid stuck up issue
857_Occurance_After.pptx
Outflow (Before) Before Inspection Frequency 5 Parts/8 Hour
857_Outflow_Before.pdf
Outflow (After) After Inspection Frequency 5 Parts/ 1 Hour
857_Outflow_After.pdf
 
11. Horizontal Deployment
Horizontal Deployment Required No
Applicable Machine / Model / Plant NA
 
12. Document Review
Documents ControlPlan, PFMEA
Specify Other Document NA
 
13. Effectiveness Of Action
Reviewed Quantity 100
Reason for submission OK