QFR No - 8000878738
Defect Details
NC No. | 8000878738 |
NC Date | 18/06/2024 |
NC Submission Date | |
Part No. | 520HK00102 |
Part Name | LIP SEAL SUPPORT |
Supplier Name & Code | 100106-SHARP ENGINEERS. |
ETL Plant | 1136-ETL Suspension Sanand |
Defect Details | DIAMETER OVER SIZE-OD OVERSIZE |
1. Problem Description
Defect Description | OD observation 51.596 mm (OD Oversize) against specification 51.556~51.575 mm. |
Detection Stage | Customer End |
Problem Severity | Fitment |
NG Quantity | 1 |
Is Defect Repeatative? | No |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | quality@sharp-engineers.com |
Plant Head/CEO Email ID | kurund.ma@sharp-engineers.com |
MD Email ID | urkhandelwal@sharp-engineers.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
2000
|
0
|
0
|
112
|
0
|
2112
|
Check Qty |
2000
|
0
|
0
|
112
|
0
|
2112
|
NG Qty |
1
|
0
|
0
|
112
|
0
|
113
|
Scrap | 1 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
All pipeline material checked for OD with Identification Tag |
3. Process Flow
Process Flow Description |
---|
Rm inward-Parting-Normalizing-CNC 1st-CNC2nd-CNC3rd-Final Inspection-PDI-Packing and Forwarding |
4. Process Details
Process / Operation | CNC |
Outsource | No |
Machine / Cell | CNC |
Machine / Cell No. | CNC |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Man | Unskilled Operator | Skilled manpower deployed | O |
Material | Incorrect RM Grade | Material found ok as per TC | O |
Method | Insert Not Change at defined frequency | Insert change at defined frequency but Part not validated by operated | X |
Method | Part not validated after replacement of insert | affect | X |
Material | Hardness Variation in RM | Hardness found ok as per specification | O |
Method | Part not clamp properly | Clamping pressure found ok as per process parameter | O |
Machine | Power cut | No effect as we are Rejecting all power cut parts | O |
Machine | Insert Broken | Operator Doing inspection with APG for ID and visual 100%. | O |
Machine | Insert Wearout | No effect | O |
Tool | Insert Change | Variation in dimensions | X |
Method | Fixture Not clean Properly | Fixture cleaning done as per SOP | O |
Man | Wrong setting done by operator | Setting done ok also setup approval report evident | O |
Material | Variation in RM OD | No effect | O |
Man | New manpower | Regular manpower deployed | O |
6. Inspection Method Analysis (Current)
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | No |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 0 |
7. Root Cause Analysis (Occurance)
Why 1 | OD oversized |
Why 2 | Observed 51.596mm against 51.556~51.575mm |
Why 3 | Insert changed and part not verify by operator and supervisor. |
Why 4 | No Pokayoke for insert life monitoring |
Why 5 | |
Root Cause (Occurance) | No Pokayoke for insert life monitoring |
Root Cause Analysis (Outflow)
Why 1 | OD oversized |
Why 2 | Skip from inspection |
Why 3 | Part not validated by operator or supervisor. |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | Part not validated by operator or supervisor. |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | Combining all CNC operation 40,50&60 in One Setup to avoid defect also New machine having pokayoke for insert change. | Manoj Kadam | 26/06/2024 | 26/06/2024 | Completed |
Outflow | Only Supervisor can Clear insert change alarm after verification of part becouse tool life programing is protected with key. | Pankaj Khadse | 26/06/2024 | 26/06/2024 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | No |
Change Details | NA |
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
10. Evidance of Countermeasure
Occurance (Before) |
No Pokayoke for insert life monitoring, 875_Occurance_Before.pdf |
Occurance (After) |
Combining all CNC operation 40,50&60 in One Setup to avoid defect also New machine having pokayoke for insert change. 875_Occurance_After.pdf |
Outflow (Before) |
Part not validated by operator or supervisor. 875_Outflow_Before.jpeg |
Outflow (After) |
Only Supervisor can Clear insert change alarm after verification of part because tool life programing is protected with key. 875_Outflow_After.jpeg |
11. Horizontal Deployment
Horizontal Deployment Required | No |
Applicable Machine / Model / Plant | NA |
12. Document Review
Documents | ControlPlan, PFMEA, WISOP, ProcessFlowChart |
Specify Other Document | NA |
13. Effectiveness Of Action
Reviewed Quantity | 5 |
Reason for submission | OD observation 51.596 mm (OD Oversize) against specification 51.556~51.575 mm |