QFR No - 8000878738
Defect Details
NC No. 8000878738
NC Date 18/06/2024
NC Submission Date
Part No. 520HK00102
Part Name LIP SEAL SUPPORT
Supplier Name & Code 100106-SHARP ENGINEERS.
ETL Plant 1136-ETL Suspension Sanand
Defect Details DIAMETER OVER SIZE-OD OVERSIZE
 
1. Problem Description
Defect Description OD observation 51.596 mm (OD Oversize) against specification 51.556~51.575 mm.
Detection Stage Customer End
Problem Severity Fitment
NG Quantity 1
Is Defect Repeatative? No
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID quality@sharp-engineers.com
Plant Head/CEO Email ID kurund.ma@sharp-engineers.com
MD Email ID urkhandelwal@sharp-engineers.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
2000
0
0
112
0
2112
Check Qty
2000
0
0
112
0
2112
NG Qty
1
0
0
112
0
113
 
Scrap 1
Rework 0
Under Deviation 0
Containment Action
All pipeline material checked for OD with Identification Tag
 
3. Process Flow
Process Flow Description
Rm inward-Parting-Normalizing-CNC 1st-CNC2nd-CNC3rd-Final Inspection-PDI-Packing and Forwarding
 
4. Process Details
Process / Operation CNC
Outsource No
Machine / Cell CNC
Machine / Cell No. CNC
5. Problem Analysis
Type Possible Cause Fact Verification Jud
ManUnskilled OperatorSkilled manpower deployedO
MaterialIncorrect RM GradeMaterial found ok as per TCO
MethodInsert Not Change at defined frequencyInsert change at defined frequency but Part not validated by operatedX
MethodPart not validated after replacement of insertaffectX
MaterialHardness Variation in RMHardness found ok as per specificationO
MethodPart not clamp properlyClamping pressure found ok as per process parameterO
MachinePower cutNo effect as we are Rejecting all power cut partsO
MachineInsert BrokenOperator Doing inspection with APG for ID and visual 100%.O
MachineInsert WearoutNo effectO
ToolInsert ChangeVariation in dimensionsX
MethodFixture Not clean ProperlyFixture cleaning done as per SOPO
ManWrong setting done by operatorSetting done ok also setup approval report evidentO
MaterialVariation in RM ODNo effectO
ManNew manpowerRegular manpower deployedO
 
6. Inspection Method Analysis (Current)
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection No
Checking Freq. Sampling
Sampling No
Sample Size 0
7. Root Cause Analysis (Occurance)
Why 1 OD oversized
Why 2 Observed 51.596mm against 51.556~51.575mm
Why 3 Insert changed and part not verify by operator and supervisor.
Why 4 No Pokayoke for insert life monitoring
Why 5
Root Cause (Occurance) No Pokayoke for insert life monitoring
 
Root Cause Analysis (Outflow)
Why 1 OD oversized
Why 2 Skip from inspection
Why 3 Part not validated by operator or supervisor.
Why 4
Why 5
Root Cause (Outflow) Part not validated by operator or supervisor.
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceCombining all CNC operation 40,50&60 in One Setup to avoid defect also New machine having pokayoke for insert change.Manoj Kadam26/06/202426/06/2024Completed
OutflowOnly Supervisor can Clear insert change alarm after verification of part becouse tool life programing is protected with key.Pankaj Khadse26/06/202426/06/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System No
Change Details NA
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) No Pokayoke for insert life monitoring,
875_Occurance_Before.pdf
Occurance (After) Combining all CNC operation 40,50&60 in One Setup to avoid defect also New machine having pokayoke for insert change.
875_Occurance_After.pdf
Outflow (Before) Part not validated by operator or supervisor.
875_Outflow_Before.jpeg
Outflow (After) Only Supervisor can Clear insert change alarm after verification of part because tool life programing is protected with key.
875_Outflow_After.jpeg
 
11. Horizontal Deployment
Horizontal Deployment Required No
Applicable Machine / Model / Plant NA
 
12. Document Review
Documents ControlPlan, PFMEA, WISOP, ProcessFlowChart
Specify Other Document NA
 
13. Effectiveness Of Action
Reviewed Quantity 5
Reason for submission OD observation 51.596 mm (OD Oversize) against specification 51.556~51.575 mm