QFR No - 8000881628
Defect Details
NC No. 8000881628
NC Date 08/07/2024
NC Submission Date
Part No. 520HL00202
Part Name OIL LOCK COLLAR
Supplier Name & Code 100176-GKN SINTER METALS PRIVATE LIMI
ETL Plant 1117-ETL K-228/9 Suspension
Defect Details NOT AS PER SPECIFICATION-CRACK
 
1. Problem Description
Defect Description Crack
Detection Stage Inprocess
Problem Severity Safety
NG Quantity 4
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID Rajendra.Sethiya@gknpm.com
Plant Head/CEO Email ID Pratik.Dharangaonkar@gknpm.com
MD Email ID Rajesh.Mirani@gknpm.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
7000
7654
0
0
0
14654
Check Qty
7000
7654
0
0
0
14654
NG Qty
2
1
0
0
0
3
 
Scrap 3
Rework 0
Under Deviation 0
Containment Action
Quality Alert raised at In process area. Awareness given to all concern stakeholders.
 
3. Process Flow
Process Flow Description
Mixing- Forming-Sintering-Steam treatment - PDI
 
4. Process Details
Process / Operation Forming
Outsource No
Machine / Cell Small Segment
Machine / Cell No. Plant 1
5. Problem Analysis
Type Possible Cause Fact Verification Jud
ManNew OpeartorOpeartor Skill Matrix verifiedO
MethodParts fallen in Rotary table due to conveyor height mismatchPast history of concerned batch verified & observed Impact genearted on OD & crack parts producedX
MaterialWrong MixMTRO
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method Sampling Inspection
Check Point at Final Inspection No
Checking Freq. Sampling
Sampling No
Sample Size 5
7. Root Cause Analysis (Occurance)
Why 1 Crack Generated on OD During Forming Process
Why 2 Impact generated on part OD on Rotary table during transferring from conveyor
Why 3 Excess gap between Rotary table & Conveyor chute end
Why 4 No checkpoint to verify Gap
Why 5
Root Cause (Occurance) Excess gap between Rotary table & Conveyor chute end resulted into excess impact on Part OD
 
Root Cause Analysis (Outflow)
Why 1 Crackparts outflown to ETL
Why 2 crack parts not detected during Inspection
Why 3 Inspection done on sampling basis
Why 4
Why 5
Root Cause (Outflow) Inspection done on sampling basis
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceGlide path provided between rotary table & conveyor clearence to avoid ImpactRohan Gunwant30/07/202430/07/2024Completed
OutflowInspection Frequency revised from 5 Parts/8 Hour to 5 Parts/1 HourRohan G30/07/202430/07/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details Inspection frequency revised from 5 Parts/8 Hour to 5 Parts/ 1 hour
Inspection Method Other
Other Inspection Method Visual
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 10
10. Evidance of Countermeasure
Occurance (Before) Excess Gap on Rotary table
918_Occurance_Before.pptx
Occurance (After) Gap Eliminated to avoid stuck up issue
918_Occurance_After.pptx
Outflow (Before) Before Inspection frequency 5 Parts/8 Hour
918_Outflow_Before.pdf
Outflow (After) After Inspection Frequency 5 Parts/ 1 Hour
918_Outflow_After.pdf
 
11. Horizontal Deployment
Horizontal Deployment Required No
Applicable Machine / Model / Plant NA
 
12. Document Review
Documents ControlPlan, PFMEA
Specify Other Document NA
 
13. Effectiveness Of Action
Reviewed Quantity 50
Reason for submission OK