QFR No - 8000881628
Defect Details
NC No. | 8000881628 |
NC Date | 08/07/2024 |
NC Submission Date | |
Part No. | 520HL00202 |
Part Name | OIL LOCK COLLAR |
Supplier Name & Code | 100176-GKN SINTER METALS PRIVATE LIMI |
ETL Plant | 1117-ETL K-228/9 Suspension |
Defect Details | NOT AS PER SPECIFICATION-CRACK |
1. Problem Description
Defect Description | Crack |
Detection Stage | Inprocess |
Problem Severity | Safety |
NG Quantity | 4 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | Rajendra.Sethiya@gknpm.com |
Plant Head/CEO Email ID | Pratik.Dharangaonkar@gknpm.com |
MD Email ID | Rajesh.Mirani@gknpm.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
7000
|
7654
|
0
|
0
|
0
|
14654
|
Check Qty |
7000
|
7654
|
0
|
0
|
0
|
14654
|
NG Qty |
2
|
1
|
0
|
0
|
0
|
3
|
Scrap | 3 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
Quality Alert raised at In process area. Awareness given to all concern stakeholders. |
3. Process Flow
Process Flow Description |
---|
Mixing- Forming-Sintering-Steam treatment - PDI |
4. Process Details
Process / Operation | Forming |
Outsource | No |
Machine / Cell | Small Segment |
Machine / Cell No. | Plant 1 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Man | New Opeartor | Opeartor Skill Matrix verified | O |
Method | Parts fallen in Rotary table due to conveyor height mismatch | Past history of concerned batch verified & observed Impact genearted on OD & crack parts produced | X |
Material | Wrong Mix | MTR | O |
6. Inspection Method Analysis (Current)
Inspection Method | Other |
Other Inspection Method | Sampling Inspection |
Check Point at Final Inspection | No |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 5 |
7. Root Cause Analysis (Occurance)
Why 1 | Crack Generated on OD During Forming Process |
Why 2 | Impact generated on part OD on Rotary table during transferring from conveyor |
Why 3 | Excess gap between Rotary table & Conveyor chute end |
Why 4 | No checkpoint to verify Gap |
Why 5 | |
Root Cause (Occurance) | Excess gap between Rotary table & Conveyor chute end resulted into excess impact on Part OD |
Root Cause Analysis (Outflow)
Why 1 | Crackparts outflown to ETL |
Why 2 | crack parts not detected during Inspection |
Why 3 | Inspection done on sampling basis |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | Inspection done on sampling basis |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | Glide path provided between rotary table & conveyor clearence to avoid Impact | Rohan Gunwant | 30/07/2024 | 30/07/2024 | Completed |
Outflow | Inspection Frequency revised from 5 Parts/8 Hour to 5 Parts/1 Hour | Rohan G | 30/07/2024 | 30/07/2024 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | Inspection frequency revised from 5 Parts/8 Hour to 5 Parts/ 1 hour |
Inspection Method | Other |
Other Inspection Method | Visual |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 10 |
10. Evidance of Countermeasure
Occurance (Before) |
Excess Gap on Rotary table 918_Occurance_Before.pptx |
Occurance (After) |
Gap Eliminated to avoid stuck up issue 918_Occurance_After.pptx |
Outflow (Before) |
Before Inspection frequency 5 Parts/8 Hour 918_Outflow_Before.pdf |
Outflow (After) |
After Inspection Frequency 5 Parts/ 1 Hour 918_Outflow_After.pdf |
11. Horizontal Deployment
Horizontal Deployment Required | No |
Applicable Machine / Model / Plant | NA |
12. Document Review
Documents | ControlPlan, PFMEA |
Specify Other Document | NA |
13. Effectiveness Of Action
Reviewed Quantity | 50 |
Reason for submission | OK |