QFR No - 8000886610
Defect Details
NC No. 8000886610
NC Date 12/08/2024
NC Submission Date
Part No. F2FQ00307B
Part Name HOLDER HANDLE LOWER P/C (XF-521)
Supplier Name & Code 201092-PRANEEL INDUSTRIES
ETL Plant 1117-ETL K-228/9 Suspension
Defect Details DENT MARK-DENT DAMAGE
 
1. Problem Description
Defect Description Dent Mark & Damage
Detection Stage Receipt
Problem Severity Aesthetic
NG Quantity 35
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID quality@praneelgroup.com
Plant Head/CEO Email ID praneelindustries@rediiffmail.com
MD Email ID anilpatil@praneelgroup.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
1216
0
0
100
0
1316
Check Qty
1216
0
0
100
0
1316
NG Qty
35
0
0
20
0
55
 
Scrap 55
Rework 0
Under Deviation 0
Containment Action
All material at ETL end and at in-house sagrigation done and NG parts are scrap at both location.
 
3. Process Flow
Process Flow Description
Raw Casting inward=>CNC Setup=>Powder Coating=>Powder Coating Inward=>VMC Setup=>De-burring=>Final Inspection=>Packing and Dispatch.
 
4. Process Details
Process / Operation VMC Machining
Outsource No
Machine / Cell VMC Machining
Machine / Cell No. VMC Cell
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MethodInadequate clamping method while machining.Verify the method of loading and unloading during machine found inadequate.X
MachineClamping pressure for part load not as per specifications.Verify the clamping pressure and found as per required specifications.O
ManSkilled person not availableVerify the skill matrix found as per skill matrix.O
MaterialMaterial specification not as per required.Vewrify the material found ok.O
ToolTooling for manufacturing the part not as per specification.Verify the machining tool and found Ok.O
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method Visual Inspection
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
7. Root Cause Analysis (Occurance)
Why 1 Dent mark-Dent Damage observed on the part.
Why 2 Clamping pressure not as per required specification on the machine.
Why 3 Clamping not done properly during the machining.
Why 4 Damage during the machining after parts unloading observed.
Why 5
Root Cause (Occurance) Damage during the machining after parts unloading observed.
 
Root Cause Analysis (Outflow)
Why 1 Dent mark-Dent Damage observed on the part.
Why 2 Parts skipped by inspector during the visual inspection.
Why 3 Awareness not available about dent and damage issue.
Why 4
Why 5
Root Cause (Outflow) Awareness not available about dent and damage issue.
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OutflowAwareness and training provided for visual inspection of the material for dent and damage issue.Mr.Yogesh Sonune19/08/202419/08/2024Completed
OccuranceTraining given to operator for air should be blow on the fixture and resting area to remove the burr.Mr.Chandrakant Nanher19/08/202419/08/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System No
Change Details ---
Inspection Method Other
Other Inspection Method Visual Inspection
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) No any work instruction for fixture cleaning in the machine work instruction.
1004_Occurance_Before.pdf
Occurance (After) Instruction for fixture cleaning with clamping and resting area added in the machine work instruction.
1004_Occurance_After.pdf
Outflow (Before) No awareness about dent and damage issue observed at ETL end.
1004_Outflow_Before.pdf
Outflow (After) Training and awareness provided for the dent and damage issue observed on the parts.
1004_Outflow_After.jpeg
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant Handle Holder Upper
 
12. Document Review
Documents WISOP
Specify Other Document Q alert,Training rec
 
13. Effectiveness Of Action
Reviewed Quantity 50
Reason for submission OK