QFR No - 8000886612
Defect Details
NC No. | 8000886612 |
NC Date | 12/08/2024 |
NC Submission Date | |
Part No. | F2BZ05712B |
Part Name | CAP OIL LOCK - J1D FF (10mm taper) |
Supplier Name & Code | 101255-MAHAVIR INDUSTRIES |
ETL Plant | 1117-ETL K-228/9 Suspension |
Defect Details | PARALITY NOT OK.-PARALLISUM FOUND NOT OK. |
1. Problem Description
Defect Description | Parallelism Found Not OK |
Detection Stage | Receipt |
Problem Severity | Fitment |
NG Quantity | 4 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | quality@mahavirind.co.in |
Plant Head/CEO Email ID | planthead@mahavirind.co.in |
MD Email ID |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
340
|
0
|
0
|
0
|
0
|
340
|
Check Qty |
340
|
0
|
0
|
0
|
0
|
340
|
NG Qty |
4
|
0
|
0
|
0
|
0
|
4
|
Scrap | 4 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
All Stages +customer End All suspected Finish Good material Verified |
3. Process Flow
Process Flow Description |
---|
R/M Inward - R/M Store- Traub parting ?10.5 ID Hole - CNC Taper Turning/ ID Boring - Bottom Side Chamfer- OD Grinding- Rust preventive washing - Final Inspection - Packing- Dispatch. |
4. Process Details
Process / Operation | CNC Taper Turning/ ID Boring |
Outsource | Yes |
Machine / Cell | CNC Section |
Machine / Cell No. | CNC-2 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Method | Not proper arrangement of Defective parts Handling on CNC Machine | Not Available Lock and Key Red box on CNC machine | X |
Man | Unskiilled Man power | Skilled operator On CNC machine | O |
Material | Hard Material | Correct Grade Material use & hardness ok | O |
Machine | CNC Machine Condition Not OK | As PM plan Check sheet Condition found ok but Chuck Jaw Boring Frequency not decide. | X |
Tool | Wrong Tool use For Pilot Drill | Correct Required Tool On CNC Machine | O |
6. Inspection Method Analysis (Current)
Inspection Method | Instrument |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
7. Root Cause Analysis (Occurance)
Why 1 | PARALITY NOT OK.-PARALLISUM FOUND NOT OK. |
Why 2 | CNC chuck jaw boring was not completed on time |
Why 3 | The operator is not aware of CNC jaw boring |
Why 4 | The frequency for jaw boring has not been decided |
Why 5 | |
Root Cause (Occurance) | The frequency for jaw boring has not been decided |
Root Cause Analysis (Outflow)
Why 1 | PARALITY NOT OK.-PARALLISUM FOUND NOT OK. |
Why 2 | Defected Part By Mistake Mix By CNC operator |
Why 3 | Improper arrangement of defective parts stored on the CNC machine. |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | Improper arrangement of defective parts stored on the CNC machine. |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | Define the frequency of CNC jaw boring and provide training to the operator. | Production Head | 14/08/2024 | 14/08/2024 | Completed |
Outflow | Arrange the lock and key in the red box on the CNC machine. | Quality head | 17/08/2024 | 17/08/2024 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | 100% |
Inspection Method | Instrument |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
10. Evidance of Countermeasure
Occurance (Before) |
The frequency for jaw boring has not been decided 1006_Occurance_Before.pptx |
Occurance (After) |
Define the frequency of CNC jaw boring and provide training to the operator. 1006_Occurance_After.jpg |
Outflow (Before) |
Improper arrangement of defective parts stored on the CNC machine. 1006_Outflow_Before.jpg |
Outflow (After) |
Arrange the lock and key in the red box on the CNC machine 1006_Outflow_After.jpg |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | All Machine and all models |
12. Document Review
Documents | PFMEA, WISOP |
Specify Other Document | no |
13. Effectiveness Of Action
Reviewed Quantity | 50 |
Reason for submission | Work instruction updated for jaw boring frequency but no revision number updated |