QFR No - 8000886612
Defect Details
NC No. 8000886612
NC Date 12/08/2024
NC Submission Date
Part No. F2BZ05712B
Part Name CAP OIL LOCK - J1D FF (10mm taper)
Supplier Name & Code 101255-MAHAVIR INDUSTRIES
ETL Plant 1117-ETL K-228/9 Suspension
Defect Details PARALITY NOT OK.-PARALLISUM FOUND NOT OK.
 
1. Problem Description
Defect Description Parallelism Found Not OK
Detection Stage Receipt
Problem Severity Fitment
NG Quantity 4
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID quality@mahavirind.co.in
Plant Head/CEO Email ID planthead@mahavirind.co.in
MD Email ID
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
340
0
0
0
0
340
Check Qty
340
0
0
0
0
340
NG Qty
4
0
0
0
0
4
 
Scrap 4
Rework 0
Under Deviation 0
Containment Action
All Stages +customer End All suspected Finish Good material Verified
 
3. Process Flow
Process Flow Description
R/M Inward - R/M Store- Traub parting ?10.5 ID Hole - CNC Taper Turning/ ID Boring - Bottom Side Chamfer- OD Grinding- Rust preventive washing - Final Inspection - Packing- Dispatch.
 
4. Process Details
Process / Operation CNC Taper Turning/ ID Boring
Outsource Yes
Machine / Cell CNC Section
Machine / Cell No. CNC-2
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MethodNot proper arrangement of Defective parts Handling on CNC MachineNot Available Lock and Key Red box on CNC machineX
ManUnskiilled Man powerSkilled operator On CNC machineO
MaterialHard MaterialCorrect Grade Material use & hardness okO
MachineCNC Machine Condition Not OKAs PM plan Check sheet Condition found ok but Chuck Jaw Boring Frequency not decide.X
ToolWrong Tool use For Pilot DrillCorrect Required Tool On CNC MachineO
 
6. Inspection Method Analysis (Current)
Inspection Method Instrument
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
7. Root Cause Analysis (Occurance)
Why 1 PARALITY NOT OK.-PARALLISUM FOUND NOT OK.
Why 2 CNC chuck jaw boring was not completed on time
Why 3 The operator is not aware of CNC jaw boring
Why 4 The frequency for jaw boring has not been decided
Why 5
Root Cause (Occurance) The frequency for jaw boring has not been decided
 
Root Cause Analysis (Outflow)
Why 1 PARALITY NOT OK.-PARALLISUM FOUND NOT OK.
Why 2 Defected Part By Mistake Mix By CNC operator
Why 3 Improper arrangement of defective parts stored on the CNC machine.
Why 4
Why 5
Root Cause (Outflow) Improper arrangement of defective parts stored on the CNC machine.
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceDefine the frequency of CNC jaw boring and provide training to the operator.Production Head14/08/202414/08/2024Completed
OutflowArrange the lock and key in the red box on the CNC machine.Quality head17/08/202417/08/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details 100%
Inspection Method Instrument
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) The frequency for jaw boring has not been decided
1006_Occurance_Before.pptx
Occurance (After) Define the frequency of CNC jaw boring and provide training to the operator.
1006_Occurance_After.jpg
Outflow (Before) Improper arrangement of defective parts stored on the CNC machine.
1006_Outflow_Before.jpg
Outflow (After) Arrange the lock and key in the red box on the CNC machine
1006_Outflow_After.jpg
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant All Machine and all models
 
12. Document Review
Documents PFMEA, WISOP
Specify Other Document no
 
13. Effectiveness Of Action
Reviewed Quantity 50
Reason for submission Work instruction updated for jaw boring frequency but no revision number updated