QFR No - 8000886662
Defect Details
NC No. | 8000886662 |
NC Date | 12/08/2024 |
NC Submission Date | |
Part No. | F2GA02302B |
Part Name | PROTECTION COVER-XF1D1-XF1C1 |
Supplier Name & Code | 100990-JAIRAJ ANCILLARIES PVT LTD |
ETL Plant | 1117-ETL K-228/9 Suspension |
Defect Details | NOT AS PER SPECIFICATION-DUST MARK |
1. Problem Description
Defect Description | Dust Mark |
Detection Stage | Customer End |
Problem Severity | Aesthetic |
NG Quantity | 694 |
Is Defect Repeatative? | No |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | planthead.aurangabad@jairajgroup.com |
Plant Head/CEO Email ID | vp@jairajgroup.com |
MD Email ID | rajiv@jairajgroup.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
14000
|
0
|
0
|
1000
|
0
|
15000
|
Check Qty |
14000
|
0
|
0
|
1000
|
0
|
15000
|
NG Qty |
694
|
0
|
0
|
35
|
0
|
729
|
Scrap | 729 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
100 % inspection at final & firewall workstation with identification mark on it . |
3. Process Flow
Process Flow Description |
---|
Injection Moulding |
4. Process Details
Process / Operation | Injection Moulding |
Outsource | No |
Machine / Cell | IM-04 |
Machine / Cell No. | IM-4 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Machine | Barrel Temp High / Low | verified as per Cp & OCS found ok , As per Standard Specification | O |
Tool | Air trapped & air vent inefficient open | verifie Air vent blocked due to carbon deposit on air vent surface | X |
Man | Man Power does not aware about this defect . | verifed that operator , In process inspector & Final Inspector does not about this defect . | X |
Material | RM Grade not as per CP . | Check with MTC & found ok as per specification | O |
Method | Sampling Inspection | verified & Found that Defect are checked on sampling basis At FI | X |
Machine | OPS & control plan not followed by Machine Operator . | verified as per CP & OCS found ok , As per standard specificiation | O |
Method | RM preheating not done | Verified as per CP & OCS found ok , As per Standard Specification | O |
6. Inspection Method Analysis (Current)
Inspection Method | Other |
Other Inspection Method | Visually |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 5 |
7. Root Cause Analysis (Occurance)
Why 1 | Dust marks due to air trapped in tool erratically while injection . |
Why 2 | Air vent blocked due to carbon deposit formed on air vent surface |
Why 3 | Carbon deposit formed due to un periodic cleaning during production |
Why 4 | Air vent cleaning done during Production is not effective . |
Why 5 | |
Root Cause (Occurance) | .Air vent cleaning done during Production is not effective . |
Root Cause Analysis (Outflow)
Why 1 | Dust mark observed on part surface . |
Why 2 | Defective part skipped from operator & final Inspector . |
Why 3 | Lack of Awareness of Highlighted defect . |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | Lack of Awareness of Highlighted defect . |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | Air vent cleaning increased from 25 pieces to 15 pieces . | Sandeep Roday | 17/08/2024 | 02/09/2024 | Completed |
Outflow | Awareness training given to in process inspector & Final Inspector about highlighted defect . | Sandeep Roday | 19/08/2024 | 02/09/2024 | Completed |
Occurance | Air vent cleaning done by Chemical WD -40 . | Ganesh Mahske | 16/08/2024 | 02/09/2024 | Completed |
Outflow | Check Point Added in PM sheet & CP & FMEA updated for the same | Sandeep Roday | 21/08/2024 | 02/09/2024 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | 100% Visual Inspection at final stage for Dust Mark |
Inspection Method | Other |
Other Inspection Method | Visual |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100 % |
10. Evidance of Countermeasure
Occurance (Before) |
Air Vent cleaning not By chemical in mould pm check sheet . 1018_Occurance_Before.xlsx |
Occurance (After) |
PM check Sheet After correction . 1018_Occurance_After.pdf |
Outflow (Before) |
Dust Mark check point not address in inspection standard . 1018_Outflow_Before.pdf |
Outflow (After) |
Dust mark check point add in inspection standard . 1018_Outflow_After.pdf |
11. Horizontal Deployment
Horizontal Deployment Required | No |
Applicable Machine / Model / Plant | NO |
12. Document Review
Documents | PMCheckSheet, WISOP, InspCheckSheet |
Specify Other Document | Q alert . |
13. Effectiveness Of Action
Reviewed Quantity | 50 |
Reason for submission | ok |