QFR No - 8000889507
Defect Details
NC No. | 8000889507 |
NC Date | 02/09/2024 |
NC Submission Date | |
Part No. | F2FQ00307B |
Part Name | HOLDER HANDLE LOWER P/C (XF-521) |
Supplier Name & Code | 201092-PRANEEL INDUSTRIES |
ETL Plant | 1117-ETL K-228/9 Suspension |
Defect Details | DENT MARK-DENT DAMAGE, PIN HOLE |
1. Problem Description
Defect Description | DENT DAMAGE |
Detection Stage | Receipt |
Problem Severity | Aesthetic |
NG Quantity | 16 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | quality@praneelgroup.com |
Plant Head/CEO Email ID | praneelindustries@rediiffmail.com |
MD Email ID | anilpatil@praneelgroup.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
350
|
0
|
0
|
0
|
200
|
550
|
Check Qty |
350
|
0
|
0
|
0
|
200
|
550
|
NG Qty |
27
|
0
|
0
|
0
|
30
|
57
|
Scrap | 57 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
All material at ETL end and In-house sagrigation done and NG parts rejected at both location. |
3. Process Flow
Process Flow Description |
---|
Raw Casting Inward=>CNC Setup=>Powder Coating=>VMC setup=>De-burring=>Final Inspection=>Packing and Dispatch. |
4. Process Details
Process / Operation | VMC Machining |
Outsource | No |
Machine / Cell | VMC Machine |
Machine / Cell No. | VMC Cell |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Machine | Clamping pressure not as per CP. | Verify clamping pressure as per CP and found OK. | O |
Tool | Toolings used for part production is not as per standard. | Verify the toolings used for part production and found adequate. | O |
Man | Unskilled manpower for inspection. | Verify skill matrix for inspector and found skilled person. | O |
Method | Inspection method not as per standard. | Verify inspection method and found inadequate. | X |
Material | Material not as per specifications. | Verify matertial composition and found as per specifications. | O |
6. Inspection Method Analysis (Current)
Inspection Method | Other |
Other Inspection Method | Visual Inspection |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | samp.plan |
7. Root Cause Analysis (Occurance)
Why 1 | Pin hole observed on the parts after powder coating. |
Why 2 | Powder used for the process contains trapped air and moisture. |
Why 3 | Degreesing bath deep time for surface cleaning is found low for cleaning the parts. |
Why 4 | |
Why 5 | |
Root Cause (Occurance) | Degreesing bath deep time for surface cleaning is found low for cleaning the parts. |
Root Cause Analysis (Outflow)
Why 1 | Pin hole observed on the parts after powder coating. |
Why 2 | Skipped from final inspection stage. |
Why 3 | Final inspector was unable to identify pin hole defect properly. |
Why 4 | Due to low lux level inspector was unable to identify the pin hole issue. |
Why 5 | |
Root Cause (Outflow) | Due to low lux level inspector was unable to identify the pin hole issue. |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Outflow | New high power LED tube installed at final inspection stage to increase the optimal lux level. | Mr. Yogesh Sonune | 12/09/2024 | 12/09/2024 | Completed |
Occurance | Degreesing bath deep time for surface cleaning increases from 5-7 min to 7-9 min for cleaning the parts. | Mr.Dhawale | 11/09/2024 | 12/09/2024 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | No |
Change Details | --- |
Inspection Method | Other |
Other Inspection Method | Visual Inspection |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
10. Evidance of Countermeasure
Occurance (Before) |
Before Degree sing bath time 5-7 min available for part cleaning process. 1064_Occurance_Before.jpeg |
Occurance (After) |
After Degree sing bath time 7-9 min done for part cleaning process. 1064_Occurance_After.jpeg |
Outflow (Before) |
Lux level on the final inspection found low for inspection and no awareness about pin hole on the parts. 1064_Outflow_Before.pptx |
Outflow (After) |
Lux level increase on the final inspection for visual inspection also awareness and training given to inspector. 1064_Outflow_After.pptx |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | Handle Holder Upper |
12. Document Review
Documents | WISOP |
Specify Other Document | Q-alert,Training rec |
13. Effectiveness Of Action
Reviewed Quantity | 50 |
Reason for submission | OK |