QFR No - 8000893358
Defect Details
NC No. 8000893358
NC Date 27/09/2024
NC Submission Date
Part No. S2MX00812B
Part Name STEEL BUSH J1A & J1D
Supplier Name & Code 101255-MAHAVIR INDUSTRIES
ETL Plant 1118-ETL E-92,93 Suspension
Defect Details LENGTH OVERSIZE-T.LENGTH O/S SPE=25.20-0.20 OBS=25.26
 
1. Problem Description
Defect Description LENGTH OVERSIZE-T.LENGTH O/S SPE=25.20-0.20 OBS=25.26
Detection Stage Inprocess
Problem Severity Fitment
NG Quantity 17
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID quality@mahavirind.co.in
Plant Head/CEO Email ID planthead@mahavirind.co.in
MD Email ID
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
7000
0
0
0
6000
13000
Check Qty
7000
0
0
0
3000
10000
NG Qty
24
0
0
0
0
24
 
Scrap 0
Rework 24
Under Deviation 0
Containment Action
All Material segregation at Customer End
 
3. Process Flow
Process Flow Description
RM inward - store - Traub Parting -Chamfering - Plating-Final inspection - Packing - Dispatch - Transport
 
4. Process Details
Process / Operation Traub Parting
Outsource Yes
Machine / Cell Traub No.1( A-25)
Machine / Cell No. Traub Section
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MachineMachine Condition Not OKAs per Daily Check sheet Machine Condition was OKO
ToolWrong Tool Insert UseCorrect carbide parting Tool Use But Tool Holding IssueX
ManUnskilled operatorAs per Skilled Matrix Operator is skilledO
MaterialWrong Grade And other grade Material UseCorrect Grade CEW-1 Material use .O
MethodMachining Process & Inspection Method WrongMachining Process is ok But Inspection Method WrongX
 
6. Inspection Method Analysis (Current)
Inspection Method Sp. Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
7. Root Cause Analysis (Occurance)
Why 1 Length oversize / under size
Why 2 During the parting process, the parting tool Insrert is lightly loose on the Traub machine.
Why 3 The tool Insert is not properly tightened because the bolt head is worn due to improper tightening with a spanner
Why 4
Why 5
Root Cause (Occurance) During the parting process, the parting tool Insert is lightly loose on the Traub machine.
 
Root Cause Analysis (Outflow)
Why 1 Length oversize / under size
Why 2 Sample Basis Inspection On final Inspection stage .
Why 3 No stage Wise Length gauges Only One Gauge For Both Stage
Why 4
Why 5
Root Cause (Outflow) No stage Wise Length gauges Only One Gauge For Both Stage
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceNew Parting Tool Holder Replace on Traub Machine and Insert change Work Instruction DisplayProduction Head28/09/202426/09/2024Completed
OutflowAdditional New Length gauge Arrange On Final Inspection Stage for 100% Inspection.Quality Head03/10/202403/10/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details 100% Length Inspection on final Stage Instead of 50% Inspection
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) During the parting process, the parting tool Insert is lightly loose on the Traub machine
1118_Occurance_Before.jpg
Occurance (After) New Parting Tool Holder Replace on Traub Machine and Insert change Work Instruction Display
1118_Occurance_After.jpg
Outflow (Before) No stage Wise Length gauges Only One Gauge For Both Stage .
1118_Outflow_Before.jpg
Outflow (After) Additional New Length gauge Arrange On Final Inspection Stage for 100% Inspection.
1118_Outflow_After.docx
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant All Steel Bush Models
 
12. Document Review
Documents ControlPlan, PFMEA, WISOP
Specify Other Document No
 
13. Effectiveness Of Action
Reviewed Quantity 150
Reason for submission after taking action no any issue observed.