QFR No - 8000893531
Defect Details
NC No. 8000893531
NC Date 27/09/2024
NC Submission Date
Part No. F2MF02702B
Part Name Spring guide Ø26 - 690 smc trial
Supplier Name & Code 100990-JAIRAJ ANCILLARIES PVT LTD
ETL Plant 1118-ETL E-92,93 Suspension
Defect Details DIAMETER OVER SIZE-O D OVER SIZE 21.0.2
 
1. Problem Description
Defect Description OD Over Size
Detection Stage Inprocess
Problem Severity Fitment
NG Quantity 102
Is Defect Repeatative? No
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID planthead.aurangabad@jairajgroup.com
Plant Head/CEO Email ID vp@jairajgroup.com
MD Email ID rajiv@jairajgroup.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
1200
0
0
500
0
1700
Check Qty
1200
0
0
500
0
1700
NG Qty
106
0
0
18
0
124
 
Scrap 124
Rework 0
Under Deviation 0
Containment Action
100 % inspection at final & firewall workstation with identification mark on it .
 
3. Process Flow
Process Flow Description
Injection Moulding
 
4. Process Details
Process / Operation Injection Moulding
Outsource No
Machine / Cell IMM09
Machine / Cell No. IMM09
5. Problem Analysis
Type Possible Cause Fact Verification Jud
ToolMould Cooling Time High/lowChecked with CP & OCS and found highX
MachineBarrel Temperature High/Lowverified as per Cp & OCS found ok , as per Standard SpecificationO
MethodSampling InspectionVerified & Found that Defect are checked on sampling basis at FIX
MachineOPS & control plan not followed by Machine OperatorVerified as per CP & OCS found ok , as per standard specificification.O
MaterialRM Grade not as per CPCheck with MTC & found ok as per specificationO
ManMan Power does not aware about this defect .Verifed that operator , In process inspector & Final Inspector aware of this defect.O
MethodChecking method for OD checkingVerified as per CP/OCS and found checking method inadequate for OD CheckingX
ToolMould Cooling Water flow rate at Cooling OutletVerified as per Tool PM checksheet and found as per specification.O
 
6. Inspection Method Analysis (Current)
Inspection Method Instrument
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 5
7. Root Cause Analysis (Occurance)
Why 1 Part OD Oversize
Why 2 Because of part not shrink as per material property
Why 3 Because of mould cooling time kept high
Why 4 Introduce the chiller system instead of normal water
Why 5 Because of in In-process cooling time was not optimum
Root Cause (Occurance) Because of in In-process cooling time was not optimum with reference to Chiller application.
 
Root Cause Analysis (Outflow)
Why 1 Because Part not detect in final inspection
Why 2 Part dimensionally check on sampling basis
Why 3 Checking method Inadequate for OD checking
Why 4
Why 5
Root Cause (Outflow) Checking method Inadequate for OD checking .
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceReduced the cooling time by 26 ± 3 second during normal water use (without chiller) and cooling time 24 ± 3 sec. during chiller use. Process Validation to be done with ref to Chiller application.Vishnu10/10/202405/10/2024Completed
OccuranceGiven training to operator to check the part in process for OD by gauge and given instruction for not to run the production if he found any out of tolerance etc.Yogesh Aharwal08/10/202405/10/2024Completed
OutflowDisplayed the Quality alert and limit sample at work Place for inspection referenceYogesh Aharwal10/10/202405/10/2024Completed
OutflowGiven on job training to Inspector to check the parts 100% for OD by OD checking gauge and Given instruction not to pass the out of spec part alsoYogesh Aharwal10/10/202405/10/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details 100% Inspection at firewall through Plug Gauge.
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) Process Cooling time as per OCS with normal cooling water
1119_Occurance_Before.pdf
Occurance (After) Training record with part checking with Plug gauge and Revised OCS with cooling time tolerance.
1119_Occurance_After.pdf
Outflow (Before) OD checking on sampling in OCS
1119_Outflow_Before.pdf
Outflow (After) Revised OCS , Quality Alert
1119_Outflow_After.pdf
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant Similar Spring Guide having insert Moulding
 
12. Document Review
Documents ControlPlan, InspCheckSheet
Specify Other Document Quality Alert, OCS
 
13. Effectiveness Of Action
Reviewed Quantity 250
Reason for submission No any issue observed in this lot.