QFR No - 8000893990
Defect Details
NC No. 8000893990
NC Date 01/10/2024
NC Submission Date
Part No. F20602602B
Part Name STEERING SHAFT - K201C
Supplier Name & Code 101228-JAIN PRECISION AND FORGINGS PV
ETL Plant 1118-ETL E-92,93 Suspension
Defect Details THREADING NOT OK-M16 THREDING U/S
 
1. Problem Description
Defect Description Threading Not Ok M16
Detection Stage Inprocess
Problem Severity Fitment
NG Quantity 6
Is Defect Repeatative? No
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID groupqaheadm134@gmail.com
Plant Head/CEO Email ID jainpfl.m134@gmail.com
MD Email ID jain@singlaforging.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
3400
0
0
500
150
4050
Check Qty
3400
0
0
500
150
4050
NG Qty
6
0
0
0
0
6
 
Scrap 6
Rework 0
Under Deviation 0
Containment Action
Immediate check the pipe line stock at ETL as well as our end and provided color code identification on each part.
 
3. Process Flow
Process Flow Description
1) Inward Insp 2) Cutting 3) Flaring 4) Boring & Facing 5) Bush Pressing 6) Welding 7) CNC - Bush boring , Threading & Facing 8) CNC - Turning 9) Buffing 10) Powder Coating 11) Inward Ins. 12) Final Inspection 13) Oiling 14) PDIR Inspection 15) Dispatch.
 
4. Process Details
Process / Operation CNC - Bush Boring & Threading
Outsource No
Machine / Cell CNC
Machine / Cell No. CNC
5. Problem Analysis
Type Possible Cause Fact Verification Jud
Tool~~~~~~O
MethodWith adjusting thread gauging inspectionWith adjusting thread gauging inspectionX
ManUnskilled OperatorLess AwarenessX
Material~~~~~~~O
MachineEntry chamfer of threading no provisionChamfer Was not given on drawingX
 
6. Inspection Method Analysis (Current)
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100/100
7. Root Cause Analysis (Occurance)
Why 1 M16 Thread Tight
Why 2 Go gauge not engaging to thread
Why 3 Chamfer of entry threading no provision
Why 4
Why 5
Root Cause (Occurance) M16 entry threading chamfer not provided .
 
Root Cause Analysis (Outflow)
Why 1 M16 Thread Tight
Why 2 Mixed up, not inspected, parts in Ok lot
Why 3 OK & not ok parts kept openly on inspection table .
Why 4 No provision to keep
Why 5
Root Cause (Outflow) Mix up not inspected parts
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceOn CNC machine bush boring Dia 14.50 mm Entry Chamfer included 1x45°. Program revisedJitendra Sahu28/09/202428/09/2024Completed
Outflow1) Inspection Table modified with divisions 2)station wise parameter & Inspector defined . 3)All material at customer end cross checkedSandeep Davane29/09/202429/09/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details Visual Inspection has been added to check entry chamfer of thread.
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100/100
10. Evidance of Countermeasure
Occurance (Before) M16 entry threading chamfer not provided .
1125_Occurance_Before.pptx
Occurance (After) On CNC machine bush boring Día 14.50 mm Entry Chamfer included 1x45°. Program revised
1125_Occurance_After.pptx
Outflow (Before) Mix up not inspected parts
1125_Outflow_Before.pptx
Outflow (After) 1)Inspection Table modified with divisions 2)station wise parameter & Inspector defined .
1125_Outflow_After.pptx
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant PRF Steering Shaft
 
12. Document Review
Documents ControlPlan, WISOP, InspCheckSheet
Specify Other Document OPL , Q Alert
 
13. Effectiveness Of Action
Reviewed Quantity 2000
Reason for submission No any threading related issue found after action taken.