QFR No - 8000895030
Defect Details
NC No. 8000895030
NC Date 08/10/2024
NC Submission Date
Part No. F800506807
Part Name UNDER BRACKET ASSY-5TSF
Supplier Name & Code 100576-SANGKAJ BRIGHT WIRES PVT LTD
ETL Plant 1117-ETL K-228/9 Suspension
Defect Details NOT AS PER SPECIFICATION-STEERING SHAFT & M6 THREAD RUSTY
 
1. Problem Description
Defect Description Under bracket rusty
Detection Stage Receipt
Problem Severity Aesthetic
NG Quantity 223
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID brightwire.qa@sangkaj.com
Plant Head/CEO Email ID steel@sangkaj.com
MD Email ID anirudh.2007@hotmail.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
600
0
0
450
225
1275
Check Qty
600
0
0
450
225
1275
NG Qty
223
0
0
0
0
223
 
Scrap 223
Rework 0
Under Deviation 0
Containment Action
1) At ETL end verified 600 Nos out of 223 nos found defective. 2) At SBWPL end verify 675 nos parts & all parts found ok. 3) For ok parts provided 100 % Verification identification marking on Top face of M6 Tapping.
 
3. Process Flow
Process Flow Description
Material Receipt - Inward inspection - Rough boring - Boss Drilling LH & RH - Ø5 Drilling - Boss Facing - Ø5 Drilling - Top Boss Tapping - Frant Boss Tapping - Bracket Slitting - Counter Drilling - Bracket Chamfering - Bracket Debarring - Shaft & bracket pressing - Shaft & bracket welding - Wire brushing - Powder coating inward - Fine boring - M6X1-6H Re-tapping - M8X1.25-6H Tapping - Final Inspection - Rust Oil Application - Packaging & Dispatch.
 
4. Process Details
Process / Operation Tapping
Outsource No
Machine / Cell Tapping
Machine / Cell No. Tapping Cell
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MethodThere was no any further provision for applying RPO inside M6 threading.Verified Not OkX
MachineUse rusty M6 TapVerified OkO
MaterialRPO Oil use non standardVerified OkO
MethodPackaging damageVerified OkO
ManInspector / Operator NewVerified OkO
ManInspector/ operator negligence-during Inspection/ processVerified Not OkX
MachineTapping Oil use non standardVerified OkO
MaterialInward Material RustyVerified OkO
MethodInventory excessVerified okO
MaterialRPO Not availableVerified OkO
MethodFIFO Not maintainedVerified okO
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method Visual Inspection
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
7. Root Cause Analysis (Occurance)
Why 1 M6X1-6H Threading Rusty
Why 2 Lack of RPO inside M6X1-6H threading.
Why 3 RPO applied only during tapping operation.
Why 4 There was no any further provision for applying RPO inside M6 threading.
Why 5
Root Cause (Occurance) There was no any further provision for applying RPO inside M6 threading.
 
Root Cause Analysis (Outflow)
Why 1 M6X1-6H Threading Rusty
Why 2 Skipped from inspector.
Why 3 Due to Inspector negligence.
Why 4
Why 5
Root Cause (Outflow) Due to Inspector negligence.
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
Occurance1.100 % RPO is to be applying inside M6 threading with the help of spl oil bottle. 2) Provided separate bin with RPO for dipping the part after final inspection. 3. Updated in the control plan & PFMEA for M6X1-6H threading Rusty.Mr. Mukesh Rathod Mr. Manoj Pathe11/10/202411/10/2024Completed
Outflow1) For ok parts provide 100 % Verification identification marking on Top face of M6 Tapping. 2) OPL displayed at tapping & final inspection stages for visual inspection.Mr. Mukesh Rathod Mr. Manoj Pathe10/10/202411/10/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System No
Change Details No change in inspection method after customer complaint
Inspection Method Other
Other Inspection Method Visual Inspection
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) RPO was applying during tapping only.
1139_Occurance_Before.xlsx
Occurance (After) 1.100 % RPO is to be applying inside M6 threading with the help of spl oil bottle. 2) Provided separate bin with RPO for dipping the part after final inspection. 3. Updated in the control plan & PFMEA for M6X1-6H threading Rusty.
1139_Occurance_After.xlsx
Outflow (Before) Identification not provided after final inspection for M6 threading rusty.
1139_Outflow_Before.xlsx
Outflow (After) 1.Provide On job Training and awareness given to all inspectors and Tapping Operator for M6X1-6gH Threading rusty & its Importance 2.Display the OPL for M6X1-6H Threading Rusty at Final inspection stage. 3.For ok parts provide 100 % Verification identification marking.
1139_Outflow_After.xlsx
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant All models
 
12. Document Review
Documents ControlPlan, PFMEA, WISOP
Specify Other Document OPL Display
 
13. Effectiveness Of Action
Reviewed Quantity 50
Reason for submission OK