QFR No - 8000896052
Defect Details
NC No. | 8000896052 |
NC Date | 17/10/2024 |
NC Submission Date | |
Part No. | F2FQ00307B |
Part Name | HOLDER HANDLE LOWER P/C (XF-521) |
Supplier Name & Code | 201092-PRANEEL INDUSTRIES |
ETL Plant | 1117-ETL K-228/9 Suspension |
Defect Details | DENT MARK-DENT DAMAGE |
1. Problem Description
Defect Description | Dent mark |
Detection Stage | Receipt |
Problem Severity | Aesthetic |
NG Quantity | 41 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | quality@praneelgroup.com |
Plant Head/CEO Email ID | praneelindustries@rediiffmail.com |
MD Email ID | anilpatil@praneelgroup.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
576
|
0
|
0
|
330
|
0
|
906
|
Check Qty |
576
|
0
|
0
|
330
|
0
|
906
|
NG Qty |
41
|
0
|
0
|
29
|
0
|
70
|
Scrap | 70 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
All material at ETL end and In-house material verify and rejected at ETL end also at in-house stage. |
3. Process Flow
Process Flow Description |
---|
Raw Casting inward=>CNC Setup=>Drilling =>Powder Coating=>Powder Coating Inward=>VMC Setup=>De-burring=>Final Inspection=>Packing and Dispatch. |
4. Process Details
Process / Operation | VMC machining |
Outsource | No |
Machine / Cell | VMC Cell |
Machine / Cell No. | VMC Machine |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Machine | Machine paramter required not as per control plan | Verify the machine parameter as clamping pressure found ok. | O |
Tool | Required tooling for part production not as per standard. | Verify the toolong for production and found adequate. | O |
Material | Material specifications not as per drawing. | Verify the material specification with MTC and found as per drawing. | O |
Man | Final inspector not as per skill matrix. | Verify the skill matrix for final inspector as well as packing person found as per skill matrix. | O |
Method | Deburring not done as per work instruction given. | Verify the deburring method by operator and found inadequate. | X |
6. Inspection Method Analysis (Current)
Inspection Method | Other |
Other Inspection Method | Visual inspection |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
7. Root Cause Analysis (Occurance)
Why 1 | Dent damage issue on the parts. |
Why 2 | Clamping pressure not as per control plan specifications. |
Why 3 | Part handling not done as per material handling WI. |
Why 4 | De-burring process not done properly as per WI. |
Why 5 | |
Root Cause (Occurance) | De-burring process not done properly as per WI. |
Root Cause Analysis (Outflow)
Why 1 | Dent damage issue on the parts. |
Why 2 | Parts skipped by inspector during final inspection. |
Why 3 | During material packing dent damage issue. |
Why 4 | Awareness not available to inspector as well as packing person for dent damage issue. |
Why 5 | |
Root Cause (Outflow) | Awareness not available to inspector as well as packing person for dent damage issue. |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Outflow | Training and awareness given to final inspector as well as packing person for dent damage issue. | Mr.Yogesh Sonune | 18/10/2024 | 18/10/2024 | Completed |
Occurance | Training given to operator of de-burring process for de-burring should be done as per WI display. | Mr. Sudarshan Kadam | 18/10/2024 | 18/10/2024 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | No |
Change Details | --- |
Inspection Method | Other |
Other Inspection Method | Visual Inspection |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
10. Evidance of Countermeasure
Occurance (Before) |
Operator not aware about dent damage issue on the parts. 1164_Occurance_Before.pptx |
Occurance (After) |
Training and awareness given to operator for de-burring on the parts. 1164_Occurance_After.pptx |
Outflow (Before) |
No any awareness about dent damage issue observed on the parts. 1164_Outflow_Before.pptx |
Outflow (After) |
Training and awareness given to final inspector for dent damage issue observed on the parts also Q alert display for the raise concern by ETL. 1164_Outflow_After.pptx |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | Handle Holder Upper |
12. Document Review
Documents | WISOP |
Specify Other Document | Q-Alert |
13. Effectiveness Of Action
Reviewed Quantity | 50 |
Reason for submission | OK |