QFR No - 8000899141
Defect Details
NC No. 8000899141
NC Date 14/11/2024
NC Submission Date
Part No. F2PA00202B
Part Name BOTTOM CASE RING RE J1A
Supplier Name & Code 100990-JAIRAJ ANCILLARIES PVT LTD
ETL Plant 1117-ETL K-228/9 Suspension
Defect Details NOT AS PER SPECIFICATION-CRACK/BROKEN
 
1. Problem Description
Defect Description CRACK/BROKEN
Detection Stage Inprocess
Problem Severity Fitment
NG Quantity 44
Is Defect Repeatative? Yes
Defect Sketch / Photo xd0zclmakc4kyvvbxutjlf4r.jpg
Supplier Communication Details
Quality Head Email ID planthead.aurangabad@jairajgroup.com
Plant Head/CEO Email ID vp@jairajgroup.com
MD Email ID rajiv@jairajgroup.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
1000
0
0
225
0
1225
Check Qty
1000
0
0
225
0
1225
NG Qty
44
0
0
12
0
56
 
Scrap 56
Rework 0
Under Deviation 0
Containment Action
Checked all available stock of 1000 no. at ETL end 100% and found 44 no. defective parts. Checked 100% all inhouse FG stock available 225 no. and found 12 no. defective parts
 
3. Process Flow
Process Flow Description
Annealing
 
4. Process Details
Process / Operation Annealing
Outsource No
Machine / Cell Annealing Tank
Machine / Cell No. ANL -01
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MaterialRM Grade not as per CP . Check withCheck with MTC & found ok as per specificationO
MachineBarrel Temp High / LowVerified as per Cp & OCS found ok , As per Standard SpecificationO
ToolAir trapped & air vent inefficient openVerified the air vent and found okO
MethodAnnealing surface volume in tank in sufficient to dip the parts in medium.Verified and found due to small tank top parts are getting float in medium .X
MethodRM preheating not doneVerified as per CP & OCS found ok , As per Standard SpecificationO
ManMan Power does not aware about this defect .Verifed that operator , In process inspector & Final Inspector aware about this defect .O
MachineOCS & control plan not followed by Machine Operator .Verified as per Cp & OCS found okO
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method Visually
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 5
7. Root Cause Analysis (Occurance)
Why 1 Parts are getting broken erratically on weld line surface.
Why 2 Parts are not getting fully dipped in annealing medium
Why 3 Due to parts are getting floated above the medium surface
Why 4 Due to Annealing tank size small , parts surface not completely annealed.
Why 5
Root Cause (Occurance) Due to Annealing tank size small , top parts surface not completely annealed resulting into insufficient annealing . Due to Annealing tank size small , parts surface not completely annealed resulting in breakages erratically.
 
Root Cause Analysis (Outflow)
Why 1 Parts are getting broken erratically on weld Line surface.
Why 2 Parts are getting skipped from Operator and Final Inspector
Why 3 After annealing process , parts are getting checked on sampling Inspection
Why 4 Lack of awareness of highlighted defect.
Why 5
Root Cause (Outflow) Lack of awareness of highlighted defect.
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceAnnealing record Register monitoring startedGanesh mhaske22/11/202422/11/2024Completed
OccuranceBig Annealing tank to Incorporate so that max parts are getting covered in one annealing cycle.Ganesh Mhaske26/11/202427/11/2024Completed
OutflowAwareness training given to in process inspector & Final Inspector about highlighted defect .Sandeep Rode22/11/202422/11/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details 100% Visual Inspection for part softness after annealing.
Inspection Method Other
Other Inspection Method Visual
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) Earlier small Annealing tank does not cover part max occupancy per cycle . Parts are getting open in medium due to floating on surface at top side which may be the probable cause .
1224_Occurance_Before.pptx
Occurance (After) Now Big Size Annealing tank implemented so that max parts are covered per cycle. Annealing Monitoring record started.
1224_Occurance_After.pdf
Outflow (Before) Earlier Parts Softness & ductility after annealing process was checked at sampling basis.
1224_Outflow_Before.pdf
Outflow (After) Parts softness and Ductility checking with 100% Inspection with OJT to In process and Firewall Inspectors.
1224_Outflow_After.pdf
 
11. Horizontal Deployment
Horizontal Deployment Required No
Applicable Machine / Model / Plant NA
 
12. Document Review
Documents ControlPlan, PFMEA, WISOP
Specify Other Document NA
 
13. Effectiveness Of Action
Reviewed Quantity 50
Reason for submission OK