QFR No - 7000851996
Defect Details
NC No. 7000851996
NC Date 27/07/2022
NC Submission Date
Part No. S2KH01502B
Part Name REBOUND SPRING K55G
Supplier Name & Code 100185-HELICAL SPRINGS
ETL Plant 1136-ETL Suspension Sanand
Defect Details SHARP EDGE & BURR-sharp Edge at end coil Id
 
1. Problem Description
Defect Description Sharp edge at end coil cutting edge towards ID
Detection Stage Receipt
Problem Severity Function
NG Quantity 1384
Is Defect Repeatative? No
Defect Sketch / Photo soaojfrmf1wdcyj03sjjik14.jpg
Supplier Communication Details
Quality Head Email ID Prabhat@helicalsprings.in
Plant Head/CEO Email ID awadhwa@helicalsprings.in
MD Email ID ataneja@helicalsprings.in
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
20000
15000
0
10000
0
45000
Check Qty
20000
15000
0
10000
0
45000
NG Qty
1384
0
0
0
0
1384
 
Scrap 1384
Rework 0
Under Deviation 0
Containment Action
Segregation of these material at customer end and our end.
 
3. Process Flow
Process Flow Description
R/M Inspection->Coiling->SR-1->Grinding->Shot peening->SR-2->Final Inspection-> Packing /Despatch
 
4. Process Details
Process / Operation Coiling
Outsource No
Machine / Cell Coiling Machine
Machine / Cell No. HTC-45B
5. Problem Analysis
Type Possible Cause Fact Verification Jud
ManCompetency level lessverify the skill matrix , competency level 4O
MachineSetting problemVerify the Set-up report found okO
Materialwire grade Ngverify the setup report found okO
Methodchecking methodverify the defect monitoring sheetO
ToolShearing tool blunttool history cardX
Materialused wrong RMverify the log found okO
Toolfeed roller was not working.verify the history card found okO
MethodNG part handling was not adequatePhysically verify the NG part handling found okO
 
6. Inspection Method Analysis (Current)
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 0
7. Root Cause Analysis (Occurance)
Why 1 Sharp edge at the End Coil ID
Why 2 Mandrill was not proper working.
Why 3 During Coiling mandrel was blunt.
Why 4 Operator was not check the mandrel Before completion of 50000 cycle.
Why 5 Mandrel Checking frequency was define 50000 cycle to cut spring after completion of 50,000 cycle than operator was checked the mandrel.
Root Cause (Occurance) After simulation , during run the machine Observed the mandrel , mandrel was blunt before completion 50000 cycle. but here mandrel checking frequency define after completion of 50000 cycle.
 
Root Cause Analysis (Outflow)
Why 1 Sharp edge at the End Coil ID
Why 2 This type of defect inspector did not capture.
Why 3 Inspector was semi skilled .
Why 4
Why 5
Root Cause (Outflow) After simulation observed the inspector negligence.
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceProvided the training all concern person.Arunesh29/07/202229/07/2022Completed
OutflowDepute the skilled personBharat01/08/202229/07/2022Completed
OutflowPoison test organisedBharat03/08/202229/07/2022Completed
OccuranceRevised the mandril frequency. 50000 replace to 40000.Sumer01/08/202229/07/2022Completed
OccuranceDisplayed the Quality alert .Bharat29/07/202229/07/2022Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System No
Change Details no
Inspection Method Other
Other Inspection Method Visual
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 0
10. Evidance of Countermeasure
Occurance (Before) Tool history card before customer complaint
210_Occurance_Before.jpg
Occurance (After) Tool history card after complaint.
210_Occurance_After.jpg
Outflow (Before) Was not fix the inspector
210_Outflow_Before.pptx
Outflow (After) Fix the operator
210_Outflow_After.pptx
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant poison test monthly plan for critical parameter and customer complaint defect.
 
12. Document Review
Documents ControlPlan, PFMEA, WISOP
Specify Other Document NO
 
13. Effectiveness Of Action
Reviewed Quantity 60000
Reason for submission 60000 nos. of Rebound spring K55G was checked 100% i.e. 2 lots in Nov 2022. No edge burr problem observed in both months of Nov 2022 & dec 2022.