QFR No - 7001024806
Defect Details
NC No. 7001024806
NC Date 18/06/2024
NC Submission Date
Part No. S2DP02902B
Part Name EXTENSION K55G
Supplier Name & Code 100106-SHARP ENGINEERS.
ETL Plant 1136-ETL Suspension Sanand
Defect Details CRACK-crack lot (suspected material )
 
1. Problem Description
Defect Description Crack
Detection Stage Inprocess
Problem Severity Safety
NG Quantity 2200
Is Defect Repeatative? No
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID quality@apw3.co.in
Plant Head/CEO Email ID kurund.ma@sharp-engineers.com
MD Email ID urkhandelwal@sharp-engineers.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
5000
5000
2000
3000
500
15500
Check Qty
5000
5000
2000
3000
500
15500
NG Qty
2200
0
0
0
5
2205
 
Scrap 2205
Rework 0
Under Deviation 0
Containment Action
Segregation done immediately for suspected material of pipeline .
 
3. Process Flow
Process Flow Description
10) RM Inward 20) RM Storage 30) Traub Operation ( Parting & Drilling) 40) Forming 50) Tapping 60) OD grinding 70) MPI 80) Visual Inspection 90) Oiling 100) Packing & forwarding
 
4. Process Details
Process / Operation Traub Machining
Outsource No
Machine / Cell Traub Machine
Machine / Cell No. SE/SSAL/06
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MethodNG storage openWrong storage method for NG part, no lock and keyX
ManUnskilled ManpowerSkill matrix as per requirementO
MachineMachine VariationJH/PM as per defined frequencyO
MaterialWrong material gradeThird part inspection as per RM testing planO
ToolTool/insert/drill worn outTool life monitoring as per defined frequencyO
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method Cross MPI
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 1:1
7. Root Cause Analysis (Occurance)
Why 1 Extension K55 Crack
Why 2 RM crack at draw stage
Why 3 Internal crack not detectable.
Why 4 Not feasible in MPI
Why 5 Need ultrasonic test at round bar stage not done.
Root Cause (Occurance) Need ultrasonic test at round bar stage not done.
 
Root Cause Analysis (Outflow)
Why 1 Crack Part got mix up with ok part
Why 2 NG material kept openly in bin without lock and keys.
Why 3 lock and key not available at MPI testing supplier (Outsource)
Why 4
Why 5
Root Cause (Outflow) lock and key not available at MPI testing supplier (Outsource)
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceUltrasonic test is being done at round bar stage after draw processMr. Ganesh Chavan25/06/202425/06/2024Completed
OutflowLock and key provided for NG material at MPI testing supplier.Mr. Shaikh L.N.26/06/202426/06/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details Ultrasonic test is being don at draw stage at sub-supplier.( Vishwa Samrudhi Industries)
Inspection Method Other
Other Inspection Method ultrasonic test (UTI
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 1:1
10. Evidance of Countermeasure
Occurance (Before) Magnetic particle inspection after draw process
874_Occurance_Before.pptx
Occurance (After) Additional Ultrasonic test is being done at round bar stage after draw process
874_Occurance_After.pptx
Outflow (Before) lock and key not available at MPI testing supplier (Outsource)
874_Outflow_Before.pptx
Outflow (After) Lock and key provided for NG material at MPI testing supplier.
874_Outflow_After.pptx
 
11. Horizontal Deployment
Horizontal Deployment Required No
Applicable Machine / Model / Plant NA
 
12. Document Review
Documents ControlPlan, PFMEA, WISOP, ProcessFlowChart, InspCheckSheet
Specify Other Document NA
 
13. Effectiveness Of Action
Reviewed Quantity 5
Reason for submission Crack