QFR No - 7001034092
Defect Details
NC No. | 7001034092 |
NC Date | 16/07/2024 |
NC Submission Date | |
Part No. | F2FA19033M |
Part Name | K0PG FORK PIPE MACHINED |
Supplier Name & Code | 101109-TUBE INVESTMENTS OF INDIA LIMI |
ETL Plant | 1136-ETL Suspension Sanand |
Defect Details | DIMETER UNDERSIZE-OD Groove Dia undersize |
1. Problem Description
Defect Description | Groove OD undersize 28.2-0.2 observed 27.85 mm |
Detection Stage | Inprocess |
Problem Severity | Fitment |
NG Quantity | 53 |
Is Defect Repeatative? | No |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | anandms@tii.murugappa.com |
Plant Head/CEO Email ID | girisha@tii.murugappa.com |
MD Email ID | mukeshahuja@tii.murugappa.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
1500
|
0
|
0
|
500
|
500
|
2500
|
Check Qty |
1500
|
0
|
0
|
500
|
500
|
2500
|
NG Qty |
53
|
0
|
0
|
0
|
0
|
53
|
Scrap | 53 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
All available material at ETL end & In-house are re - inspected with Snap Gauge. |
3. Process Flow
Process Flow Description |
---|
INWARD - CNC MACHINING - DRILLING - DIBURRING - FINAL INSPECTION - PACKING - DISPATCH TO ETL. |
4. Process Details
Process / Operation | CNC Machining |
Outsource | No |
Machine / Cell | Cell No -3 |
Machine / Cell No. | Cell No -3 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Method | Inspection Frequency | Verified records and observed that component inspected at the time of setup & every Hour | O |
Tool | Insert Broken | discussion with operator there was insert broken incidence. Operator has not checked parts produced | X |
Method | Machining Parameter | Verified through Gemba observation and found all Machine Parameter as per Control Plan | O |
Material | Raw tube OD U/s | Verified & found ok | O |
6. Inspection Method Analysis (Current)
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 5 nos Hour |
7. Root Cause Analysis (Occurance)
Why 1 | Groove OD Dim. 28.2-0.2 mm found under size observed 27.85 mm at Customer end. |
Why 2 | Groove OD Dim. 28.2-0.2 mm under size during CNC Machining process due to CNC Insert Point broken before changing frequency. |
Why 3 | due to burr/ chips interrupted bet Insert point & material |
Why 4 | Insufficient coolant flow on insert point. |
Why 5 | Coolant pipe partially chock -up. |
Root Cause (Occurance) | Coolant pipe partially chock -up. |
Root Cause Analysis (Outflow)
Why 1 | Groove OD Dim. 28.2-0.2 mm found under size observed 27.85 mm at Customer end. |
Why 2 | Escape from Inspection |
Why 3 | No inspection at Final Inspection for groove OD Size. |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | No inspection at Final Inspection for groove OD Size. |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Outflow | inspection point added at Final Inspection for groove OD Size on sampling basis with snap Gauge | Mr. Abishek Yadav | 02/08/2024 | 22/07/2024 | Completed |
Occurance | Coolant pipe choke -up corrected. | Mr. Palak | 02/08/2024 | 22/07/2024 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | inspection point added at Final Inspection for groove OD Size on sampling basis with snap Gauge |
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | after 5 no |
10. Evidance of Countermeasure
Occurance (Before) |
Coolant pipe Partially Choke -up. 942_Occurance_Before.pptx |
Occurance (After) |
Coolant pipe Partially Choke -up cleared 942_Occurance_After.pptx |
Outflow (Before) |
No Inspection at Final Inspection 942_Outflow_Before.pptx |
Outflow (After) |
Quality alert displayed at Final Inspection for Check after every 05 Nos with snap gauge & Training provided for inspector & operator. 942_Outflow_After.pptx |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | K-86 -A |
12. Document Review
Documents | WISOP |
Specify Other Document | NO |
13. Effectiveness Of Action
Reviewed Quantity | 5 |
Reason for submission | Groove OD undersize 28.2-0.2 observed 27.85 mm |