QFR No - 7001036712
Defect Details
NC No. | 7001036712 |
NC Date | 25/07/2024 |
NC Submission Date | |
Part No. | F2FA19033M |
Part Name | K0PG FORK PIPE MACHINED |
Supplier Name & Code | 101109-TUBE INVESTMENTS OF INDIA LIMI |
ETL Plant | 1136-ETL Suspension Sanand |
Defect Details | LENGTH UNDERSIZE-Short Lenght (287.43) |
1. Problem Description
Defect Description | Specification 288.3+0.2/-0.2 observation 287.43 undersize. |
Detection Stage | Receipt |
Problem Severity | Fitment |
NG Quantity | 1005 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | anandms@tii.murugappa.com |
Plant Head/CEO Email ID | girisha@tii.murugappa.com |
MD Email ID | mukeshahuja@tii.murugappa.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
1005
|
0
|
0
|
1000
|
500
|
2505
|
Check Qty |
1005
|
0
|
0
|
1000
|
500
|
2505
|
NG Qty |
1
|
0
|
0
|
0
|
0
|
1
|
Scrap | 1 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
All available material at ETL end & In-house are re - inspected with Conventional Length Gauge. |
3. Process Flow
Process Flow Description |
---|
INWARD - CNC MACHINING - DRILLING - DIBURRING - FINAL INSPECTION - PACKING - DISPATCH TO ETL. |
4. Process Details
Process / Operation | CNC MACHINING |
Outsource | No |
Machine / Cell | CELL N0 -5 |
Machine / Cell No. | CELL N0 -5 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Material | Raw tube length U/s | Verified Records & found ok | O |
Man | Tube come back due to Back Pressure | Verified through Gamba &found Tube come back due to Back Pressure. Operator has to Judge for resting | X |
Machine | Machine Parameter | Verified through Gemba observation and found all Machine Parameter as per Control Plan | O |
Method | Wrong Setup | Verified Setup Reports & found OK. | O |
6. Inspection Method Analysis (Current)
Inspection Method | Pokayoke |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | sampleplan |
7. Root Cause Analysis (Occurance)
Why 1 | Length under size found at customer end (Specification 288.3+0.2/-0.2 observation 287.63 mm ) |
Why 2 | Excess Material cut during Tube facing operation in CNC Machining. |
Why 3 | Tube hold away from Stopper. |
Why 4 | Tube come back due to Back Pressure. Operator has to Judge for resting on Stopper |
Why 5 | |
Root Cause (Occurance) | Tube come back due to Back Pressure. Operator has to Judge for resting on Stopper |
Root Cause Analysis (Outflow)
Why 1 | Length under size found at customer end (Specification 288.3+0.2/-0.2 observation 287.63 mm ) |
Why 2 | skip from proxy Sensor on Drilling M/c & 100 % conventional length gauge |
Why 3 | |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | skip from 100 % conventional length gauge |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Outflow | OK & Not OK Master sample made for verification of conventional length gauge. | Abishek Yadav | 06/08/2024 | 05/08/2024 | Completed |
Occurance | Additional Tool added on CNC m/c Tool Head for Tube resting on Stopper on Cell No - 05. | Palak Shah | 06/08/2024 | 05/08/2024 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | 100 % Inspection with Conventional Length Gauge for Next 1 Month. |
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
10. Evidance of Countermeasure
Occurance (Before) |
Tube come back due to Back Pressure. Operator has to Judge for resting on Stopper. No Provision to ensure 965_Occurance_Before.pptx |
Occurance (After) |
Additional Tool added on CNC m/c Tool Head for Tube resting on Stopper 965_Occurance_After.pptx |
Outflow (Before) |
No Master samples of OK & NOT OK tube for Verification at Final Inspection 965_Outflow_Before.pptx |
Outflow (After) |
Master samples of OK & NOT OK tube made for Verification at Final Inspection 965_Outflow_After.pptx |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | all Simians control Machines. |
12. Document Review
Documents | InspCheckSheet |
Specify Other Document | NO |
13. Effectiveness Of Action
Reviewed Quantity | 5 |
Reason for submission | Specification 288.3+0.2/-0.2 observation 287.43 undersize |