QFR No - 7001085484
Defect Details
NC No. 7001085484
NC Date 26/12/2024
NC Submission Date
Part No. B2GQ01903O
Part Name MASTER CYLINDER RAW CASTING- C101 H
Supplier Name & Code 101180-MAULI CAST TECH PVT. LTD
ETL Plant 1120-ETL K-226/2 Disc Brakes
Defect Details DIMENSSIONAL DEFECT-Pocket ID undersize
 
1. Problem Description
Defect Description Pocket ID Oversize
Detection Stage Receipt
Problem Severity Fitment
NG Quantity 1008
Is Defect Repeatative? Yes
Defect Sketch / Photo qlasf0aite00ai1he1jwotfc.jpg
Supplier Communication Details
Quality Head Email ID quality@maulicasttech.com
Plant Head/CEO Email ID planthead@maulicasttech.com
MD Email ID shrikant.shelke@maulimetal.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
1008
0
0
0
2508
3516
Check Qty
1008
0
0
0
2508
3516
NG Qty
1008
0
0
0
0
1008
 
Scrap 0
Rework 1008
Under Deviation 0
Containment Action
1.ETL End – 1008 Qty 2.Available stock at Supplier end 100% verification started for Dimn 28 & 46 (2508 no’s in WIP At MCTPL End) 3.Awareness given to all concern person with Q alert. 4.100% gauges inspection started at final inspection stage with Dot marking. 5.Provided gauge & 100% inspection started at final inspection stage.
 
3. Process Flow
Process Flow Description
Raw material Receipt & Inspection of Alloy - Raw Material Storage -Melting of Aluminum Alloy -Gravity Die Casting -Gate & Riser cutting-Lancering-Fettling -Heat Treatment -T6-Shot Blasting-Tracebility -Final Visual Inspection-Pre- Dispatch Inspection -Packing & Dispatch .
 
4. Process Details
Process / Operation GDC OPERATION
Outsource No
Machine / Cell GDC MACHINE
Machine / Cell No. GDC MACHINE -14
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MethodLoose insert dimension is in lower side due to Pocket punch wear out during running.After recheck the part dimension found in lower side.X
ToolPocket punch wear outPocket punch wear out due to frequent polishing on punch surface Punch Wear out By 0.020 mm to 0.X
ManSkipped from in process inspection.nspector checked as per drawing by vernier and not detected 20 micron variation by VCX
 
6. Inspection Method Analysis (Current)
Inspection Method Instrument
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
7. Root Cause Analysis (Occurance)
Why 1 Found go gauge not passing in RFD part _Dimn. 46+0.2-DR and 28+0.2-DR Under size
Why 2 Go gauge Not passing completely
Why 3 Pocket Dimn found under size by 0.020 to 0.040 mm.
Why 4 Pocket punch wear out during running ( Wear out by 10400 shots).
Why 5 Tool wear out early as decided tool life due to Pocket punch wear out due to frequent polishing on punch surface .
Root Cause (Occurance) Tool wear out early as decided tool life due to Pocket punch wear out due to frequent polishing on punch surface .
 
Root Cause Analysis (Outflow)
Why 1 Skipped from in process inspection .
Why 2 Dimn. checked but not detected by 10 to 20 micron during inspection.
Why 3 This dimn. checked by vernier .
Why 4 This is pocket profile dimn. So Inspection method is wrong -because dimn. checked by vernier .
Why 5
Root Cause (Outflow) 10 to 20 micron not detected during in process inspection .
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
Occurance1.Die life monitoring started and Punch life to be fixed ( Now Tool life decided 10400 shots ). 2.New punch to be procured for maintaining min max stock.Pradip Benurkar.31/01/202507/01/2025Completed
Outflow1.Provided gauge & 100% inspection started at final inspection stage. 2.This pocket Dimn. Check by profile gauge during in process inspection & setup.Nadeem Shaikh24/12/202424/12/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details Provided gauge & 100% inspection started at final inspection stage and This pocket Dimn. Check by profile gauge during in process inspection & setup.
Inspection Method Sp. Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) Go gauge Not passing completely. Pocket punch wear out due to frequent polishing on punch surface
1293_Occurance_Before.pptx
Occurance (After) 1.Tool/punch life monitoring started and Punch life to be fixed (Now Punch life decided is 10400 shots ). 2. New punch to be procured for maintaining min max stock
1293_Occurance_After.pptx
Outflow (Before) Inner pocket dimn. 46+0.2-DR and 28+0.2-DR found not ok (Under size, pocket gauge not passing completely, All 4 cavity)-
1293_Outflow_Before.png
Outflow (After) 1. Provided gauge & 100% inspection started at final inspection stage. 2.This Dimn. Check by special profile gauge during setup & in-process inspection.
1293_Outflow_After.png
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant TVS FRONT MASTER CLY.
 
12. Document Review
Documents ControlPlan, PMCheckSheet, InspCheckSheet
Specify Other Document Tool life sheet
 
13. Effectiveness Of Action
Reviewed Quantity
Reason for submission