QFR No - 8000783853
Defect Details
NC No. 8000783853
NC Date 14/04/2022
NC Submission Date
Part No. 550BZ04302
Part Name CAP OIL LOCK - DT
Supplier Name & Code 100106-SHARP ENGINEERS.
ETL Plant 1117-ETL K-228/9 Suspension
Defect Details NOT AS PER SPECIFICATION-PARALLELISM NOT OK
 
1. Problem Description
Defect Description End Face Parallelism Not Ok
Detection Stage Receipt
Problem Severity Function
NG Quantity 144
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID quality@apw3.co.in
Plant Head/CEO Email ID kurund.ma@sharp-engineers.com
MD Email ID urkhandelwal@sharp-engineers.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
900
0
0
0
0
900
Check Qty
900
0
0
0
0
900
NG Qty
68
0
0
0
0
68
 
Scrap 0
Rework 68
Under Deviation 0
Containment Action
Under cut added in three chuck jaw for burr removing .
 
3. Process Flow
Process Flow Description
CNC stage
 
4. Process Details
Process / Operation CNC Machining
Outsource No
Machine / Cell Machine Chop
Machine / Cell No. SE/CNCE/04
5. Problem Analysis
Type Possible Cause Fact Verification Jud
ManUnskilled operatorSkill matrix monitoringO
ToolInsert Worn outTool life monitoringO
MaterialWrong materialMTC & Third party reportO
MachineThree chuck jaw under cutMissingX
MethodImproper loadingObservedX
 
6. Inspection Method Analysis (Current)
Inspection Method Sp. Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 10:100
7. Root Cause Analysis (Occurance)
Why 1 0.02mm PARALLELISM NOT OK
Why 2 Improper part loading
Why 3 Less under cut in chuck jaw
Why 4 Under cut removed while jaw boring
Why 5
Root Cause (Occurance) Under cut removed while jaw boring
 
Root Cause Analysis (Outflow)
Why 1 Excess parallelism
Why 2 Sampling basis inspection as per IS:2500
Why 3 Following checking frequency as per defined control plan
Why 4
Why 5
Root Cause (Outflow) Following checking frequency as per defined control plan (32:1200 Nos.)
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
Outflow100% inspection started before dispatchMr. Shaikh L.N.20/04/202220/04/2022Completed
Occurance2mm under cut added in chuck jawMr. Pandhre Datta20/04/202220/04/2022Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details Checking frequency defined 100:1000
Inspection Method Sp. Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 100:1000
10. Evidance of Countermeasure
Occurance (Before) Burr cleaning done thru air pressure , improper cleaning because there is no under cut in clamping chuck jaw, burr, chip not removed from Chuck jaw properly.
50_Occurance_Before.pptx
Occurance (After) Cleaning started thru air gun by providing high air pressure (4 Bar), burr chip removed from chuck jaw properly and defect eliminated because under cut added up to 1.5mm.
50_Occurance_After.pptx
Outflow (Before) Sampling basis inspection as per IS:2500 (Sample size 32:1200 as per IS:2500)
50_Outflow_Before.jpg
Outflow (After) Sample size increased from 32:1200 to 100:1200 Nos.
50_Outflow_After.jpg
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant CAP OIL LOCK J1D
 
12. Document Review
Documents ControlPlan
Specify Other Document -
 
13. Effectiveness Of Action
Reviewed Quantity 300
Reason for submission Next 2 lot inspected and no defect found