QFR No - 8000808079
Defect Details
NC No. 8000808079
NC Date 17/10/2022
NC Submission Date
Part No. S2HT68607B
Part Name OUTER SPRING K23L
Supplier Name & Code 101069-SAGAR SPRINGS PVT LTD
ETL Plant 1116-ETL K-120 Suspension
Defect Details HOOK MARK-TOUCHUP NOT OK
 
1. Problem Description
Defect Description Powder coating observed not OK in almost all model & on daily basis. In K23L Outer spring supplied for expert, due to hook mark concern, end customer raising complaint on frequently.
Detection Stage Inprocess
Problem Severity Aesthetic
NG Quantity 28
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID quality@sagarsprings.com
Plant Head/CEO Email ID ajai.singh@sagarsprings.com
MD Email ID sagar@sagarsprings.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
1500
5000
0
1600
0
8100
Check Qty
1500
5000
0
1600
0
8100
NG Qty
28
450
0
100
0
578
 
Scrap 0
Rework 578
Under Deviation 0
Containment Action
Segregation carried out at warehouse as well as FG and spring hook mark reworked
 
3. Process Flow
Process Flow Description
Coiling – Tempering – Grinding - Shot Pinning – Tempering – Scragging – Sq correction/ht checking –Pre treatment-Powder coating- Inspection-Dispatch
 
4. Process Details
Process / Operation Inspection
Outsource No
Machine / Cell Inspection and touch up table
Machine / Cell No. 130
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MaterialImproper hookFound hook used are of appropriate designO
MethodSpring not hanged properlySpring are hanged properly on hanger and locked properlyO
MaterialHook get deformed while locking of springIn case of using used hook, some time hook shape get deformedX
MethodUsed hook with powder usedFound hook used are bared not powder coatedO
ManLoading person negliganceFound some loading operators not properly loading springX
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method Visual Inspection
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
7. Root Cause Analysis (Occurance)
Why 1 Hook get deformed while locking of spring
Why 2 Hook strength of some hooks get weakens because of excessive reuse
Why 3 Used hook with more than 4 cycle get mixed
Why 4
Why 5
Root Cause (Occurance) Used hook with more than 4 cycle get mixed with other hook
 
Root Cause Analysis (Outflow)
Why 1 Spring is not hanged properly and locked properly
Why 2 Loading operator negilgence
Why 3 Absence of awareness in loading person
Why 4
Why 5
Root Cause (Outflow) Absence of awareness in loading person result in improper loading
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceProper arrangement of hook made to identify it burning frequency and it statusPC-Supervisor22/10/202222/10/2022Completed
OutflowRefresher training will be given to loading operator for checking loading pattern and proper lockingPC-Supervisor19/10/202219/10/2022Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details Proper visual inspection at loading stage
Inspection Method Other
Other Inspection Method Visual inspection
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) Hook of more than 3 burnt get mix and deformed hook get used on line
287_Occurance_Before.pdf
Occurance (After) Hook are properly tracked and it freq could be identified it remain well arranged
287_Occurance_After.pdf
Outflow (Before) Lack of awareness to Loading person and Inspector
287_Outflow_Before.pdf
Outflow (After) Operators and inspectors are well understood and loading spring properly and identify hook mark defective spring
287_Outflow_After.pdf
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant Applicable to all the powder coated springs
 
12. Document Review
Documents ControlPlan, PFMEA, WISOP
Specify Other Document OPL
 
13. Effectiveness Of Action
Reviewed Quantity 1000
Reason for submission Completed