QFR No - 8000832953
Defect Details
NC No. 8000832953
NC Date 15/06/2023
NC Submission Date
Part No. 520AE01502
Part Name CORE PLATE LML
Supplier Name & Code 100959-AAR CEE ENGINEERING WORKS UNIT
ETL Plant 1132-ETL K-226/1 TRANSMISSION
Defect Details DAMAGES-CLAW WIDTH 15.+/-0.05 O/S 16.24 & DAMAGE
 
1. Problem Description
Defect Description LML Core Plate damage at claw & Width gets oversize upto 16.24 mm against 15.8±0.05 mm (Fitment issue )
Detection Stage Inprocess
Problem Severity Fitment
NG Quantity 2
Is Defect Repeatative? Yes
Defect Sketch / Photo afg4miylhknnpxt5w1xiz25m.jpg
Supplier Communication Details
Quality Head Email ID qc@aarceeengg.com
Plant Head/CEO Email ID qc@aarceeengg.com
MD Email ID vaibhav.arora@aarceeengg.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
10000
25000
15000
10000
0
60000
Check Qty
10000
25000
15000
10000
0
60000
NG Qty
10
0
0
0
0
10
 
Scrap 10
Rework 0
Under Deviation 0
Containment Action
All material hold and segregated with marking
 
3. Process Flow
Process Flow Description
RM receive +RM Store+ Holding cum molting +HPDC+Trimming Ist+Trimming 2nd +shot blasting +Stress reliving + Final inspection+ Sound test
 
4. Process Details
Process / Operation trimming
Outsource No
Machine / Cell power press
Machine / Cell No. 30 ton
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MethodImproper tool settingObserved setting done properly by tool setter(WI/PRM/002) F31/QAD(HIR-TRIM)O
Methodimproper checking methodcheckd by vernier caliper during set-up & in-process inspection , But possibility is there to bypassX
Methodpart stuck in trimming toolObserved part no chance of stucking in tool(WI/PRM/002)O
MachineTrimming tool bluntChecked reshaping frequency proper adhered found okO
MachineInsufficient air pressureObserved pressure was 4 kg/cm2 found ok (WI/PRM/002)O
MethodImproper method used for part remove from machinePart not proper remove from back side ,chance of width overX
MachineTrimming machine not working properlyAs per machine check sheet found okO
 
6. Inspection Method Analysis (Current)
Inspection Method Instrument
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 5 pcs /2hr
7. Root Cause Analysis (Occurance)
Why 1 Trimming part stucked in tool ,chance of claw width over
Why 2 Sometime parts get stuck up in Die after trimming and does not fly even puff of air. Operator keep running the machine continue, then core plate lug pressed by punch and claw width size become over.
Why 3 There is narrow space for the trimming tool to come off when the part is stuck
Why 4 No provision in tool to avoid such type issue
Why 5 Claw width oversize possibility not considered as an failure mode in PFMEA during trimming
Root Cause (Occurance) Claw width oversize possibility not considered as an failure mode in PFMEA during trimming
 
Root Cause Analysis (Outflow)
Why 1 Checking method not sufficient to detect claw width over size on one claw at trimming & PDI
Why 2 Claw width checked by vernier caliper ,during set-up, houlry & PDI, which does not ensure of whole lot /parts
Why 3 Claw width oversized (One claw) possibility not considered while defined in control plan
Why 4 No criteria for defining the inspection method in control plan
Why 5 Procedure not available for control plan & inspection standard
Root Cause (Outflow) Procedure not available for control plan & inspection standard
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccurancePart ejection system to be made in trimming tool to avoid stuck issueRadhesyam02/11/202302/11/2023Completed
OutflowControl Plan to be updated-Ajay Malik02/11/202302/11/2023Completed
OccurancePFMEA updated for claw width oversize at one clawAjay Malik02/11/202302/11/2023Completed
OutflowInspection method improvedAjay Malik02/11/202302/11/2023Completed
OutflowPoison test to be done to verify the effectiveness of inspection-Ajay Malik02/11/202302/11/2023Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System No
Change Details NO CHANGE
Inspection Method Instrument
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 20 nos/hr
10. Evidance of Countermeasure
Occurance (Before) NO TRAINING RECORD
479_Occurance_Before.jpg
Occurance (After) TRAINING GIVEN TO THE OPERATOR
479_Occurance_After.pdf
Outflow (Before) Inspection method poor
479_Outflow_Before.pdf
Outflow (After) Indexing gauge implemented
479_Outflow_After.pptx
 
11. Horizontal Deployment
Horizontal Deployment Required No
Applicable Machine / Model / Plant NO CHANGE
 
12. Document Review
Documents ControlPlan, PFMEA
Specify Other Document NO
 
13. Effectiveness Of Action
Reviewed Quantity 10000
Reason for submission Root Cause analysis not co-relate to defect phenomenon -Possibility of Core plate press during trimming operation