QFR No - 8000834882
Defect Details
NC No. 8000834882
NC Date 28/06/2023
NC Submission Date
Part No. S2AB04412B
Part Name PRELOAD ADJUSTER
Supplier Name & Code 101273-SAPTAGIRI ENGINEERING PRIVATE
ETL Plant 1116-ETL K-120 Suspension
Defect Details WELDING NOT OK-WELDING DEFECT
 
1. Problem Description
Defect Description Welding NG concern.- Welding incomplete, Blow holes, etc.
Detection Stage Receipt
Problem Severity Aesthetic
NG Quantity 228
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID quality@saptagirigroup.in
Plant Head/CEO Email ID production@saptagirigroup.in
MD Email ID
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
2000
0
0
0
0
2000
Check Qty
2000
0
0
0
0
2000
NG Qty
228
0
0
0
0
228
 
Scrap 228
Rework 0
Under Deviation 0
Containment Action
100 % material verified
 
3. Process Flow
Process Flow Description
Raw material welding + sheet shearing + Blanking + U bending + First rounding + Second rounding + CO2 welding (single spot) + CO2 welding (Full run) + Weld bead turning & grinding + Buffing + Parting & ID chamfer + Single notch + First flaring + Second flaring + Restracking + OD trimming & 8 nos notching + Face deburring + Buffing + Fe Zn plating + Final inspection + Packing/ storing.
 
4. Process Details
Process / Operation Co2 welding opeartion
Outsource No
Machine / Cell 01
Machine / Cell No. 01
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MachineRound Bending not uniform (Circular)Round bending observe uniform ( Circular )O
MethodSample basis InspectionWhile welding and buffing operation only do the sample basis inspectionX
MachineExcess welding outside the gapNo Excess buffing observedO
MachineUneven round bendingHeight variation in both side as well as uneven gapX
MachineRound bending gap unevenIn a few part observed uneven gap at top side less ( 0.54 mm ) and bottom side more (1.44 mmX
MachineUneven WeldingWelding run verified and observed evenly ( In straight line )X
MachineGap not filled by weldingGap fully filled by welding operationO
MachineExcess buffing on welding bead areaNo Excess buffing on welding lineO
ManLess awarenessOperator and inspector not aware about the weld line openO
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method Visual
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100 %
7. Root Cause Analysis (Occurance)
Why 1 Welding Open after buffing operation
Why 2 Uneven welding fusion or uneven welding filling done
Why 3 Uneven welding gap
Why 4 Uneven round bending
Why 5 Ram entry less or raw material spring back
Root Cause (Occurance) 1. Uneven round bending / Round bending gap uneven 2. Ram entry less or raw material spring back
 
Root Cause Analysis (Outflow)
Why 1 Welding Open after buffing operation
Why 2 No Inspection after the buffing operation.
Why 3
Why 4
Why 5
Root Cause (Outflow) No Inspection after the buffing operation.
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
Occurance100% inspection starts after welding operation.Mr. Munja Hore30/06/202329/06/2023Completed
OccuranceDraw route process to be introduce instead of welding process.Mr. Ramdas Chavan30/06/202329/06/2023Completed
OutflowQ-Alert display at Final inspection and welding stage.Mr. Munja Hore30/06/202329/06/2023Completed
Outflowfor ID verification Gauge provided after round bending and re stackingMr. Munja Hore30/06/202329/06/2023Completed
OccuranceRe stacking operation started after round bending to uneven gapMr. Ramdas Chavan30/06/202329/06/2023Completed
OccuranceBefore Welding operation 100% inspection starts for uneven round bend.Mr. Munja Hore30/06/202329/06/2023Completed
Outflow200% Inspection started along with marking at inner side at Final InspectionMr. Munja Hore30/06/202329/06/2023Completed
OutflowTraining given concern operator and inspector for uneven bending and welding open after the buffing process.Mr. Munja Hore30/06/202329/06/2023Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System No
Change Details NA
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100 %
10. Evidance of Countermeasure
Occurance (Before) Action plan
501_Occurance_Before.pptx
Occurance (After) Action plan
501_Occurance_After.pptx
Outflow (Before) Comparison of welded and without welded parts
501_Outflow_Before.pdf
Outflow (After) Comparison of welded and without welded parts
501_Outflow_After.pdf
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant Other adjuster also ( Re- J1a)
 
12. Document Review
Documents ControlPlan, PFMEA, ProcessFlowChart
Specify Other Document Comparison report
 
13. Effectiveness Of Action
Reviewed Quantity 10
Reason for submission Ok