QFR No - 8000853049
Defect Details
NC No. | 8000853049 |
NC Date | 28/11/2023 |
NC Submission Date | |
Part No. | S2HT49207B |
Part Name | OUTER SPRING SILVER- AAGM |
Supplier Name & Code | 100186-SAGAR SPRINGS PRIVATE LIMITED |
ETL Plant | 1143-ETL Suspension Halol, Vadodara |
Defect Details | POWDER COATING NOT OK-RUBBING MARK |
1. Problem Description
Defect Description | RUBBING MARK AND SCRATCH MARK IN AAGM SILVER OUTER SPRING |
Detection Stage | Inprocess |
Problem Severity | Aesthetic |
NG Quantity | 490 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo | dhsnflow3mtppp15idcmtd4b.jpg |
Supplier Communication Details
Quality Head Email ID | quality@sagarsprings.com |
Plant Head/CEO Email ID | ajai.singh@sagarsprings.com |
MD Email ID | sagar@sagarsprings.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
1980
|
0
|
0
|
280
|
0
|
2260
|
Check Qty |
1980
|
0
|
0
|
280
|
0
|
2260
|
NG Qty |
490
|
0
|
0
|
0
|
0
|
490
|
Scrap | 0 |
Rework | 490 |
Under Deviation | 0 |
Containment Action |
---|
SSPL represntative visited ETL verify the problem and segregated spring at ETL end 490 nos recall to sagar springs and will be recovered |
3. Process Flow
Process Flow Description |
---|
coil-tempring,end grinding-shot pinning-tempring-sq connection Htchecking-pre-treatment-powder coating-inspection-packing-dispatch |
4. Process Details
Process / Operation | Packing |
Outsource | No |
Machine / Cell | Packing |
Machine / Cell No. | 130 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Man | Person negligence on spring handling | Found persons are aware and handling it properl | O |
Material | Powder deffective | Found powder is OK as problem is not 100% | O |
Method | Packing method is not adequate | Spring is packed in box which is tight which result in to rubbing mark | X |
6. Inspection Method Analysis (Current)
Inspection Method | Other |
Other Inspection Method | Visual inspection |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
7. Root Cause Analysis (Occurance)
Why 1 | Rubbing mark on silver spring |
Why 2 | Spring outer surface is get rubbed hardly |
Why 3 | Spring is packed in corrugated box with 30 nos honey comb interlock is tight |
Why 4 | Bin for spring is not available as regular bins area short in height while spring height is more |
Why 5 | |
Root Cause (Occurance) | Spring pack in corrugated box which is tight and same bin for particular spring is not available |
Root Cause Analysis (Outflow)
Why 1 | Spring with rubbing mark move to customer |
Why 2 | Rubbing mark generated after packing hence it is not detected |
Why 3 | |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | Rubbing mark generate after packing in corrugated box |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | Bin with proper height with plastic insert will be developed and same will be introduced for packing | Powder Coating Supervisor | 31/12/2023 | 28/12/2023 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | No |
Change Details | As rubbing mark is in packing hence packing mode is change so there is no need in change in inspection method |
Inspection Method | Other |
Other Inspection Method | Visual Inspection |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
10. Evidance of Countermeasure
Occurance (Before) |
Earlier springs was dispatched in corrugated box which remain tight and generate black rubbing mark on spring Outer surface 601_Occurance_Before.pdf |
Occurance (After) |
Started packing and dispatch spring in Plastic with PP interlock to avoid rubbing mark 601_Occurance_After.pdf |
Outflow (Before) |
Spring is checked and rubbing mark generates after packing hence it not get detected 601_Outflow_Before.pdf |
Outflow (After) |
One point lesson given to inspector and started sampling checking of packed spring 601_Outflow_After.pdf |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | All powder coated spring with metallic silver paint |
12. Document Review
Documents | ControlPlan, PackingStd |
Specify Other Document | Packing std |
13. Effectiveness Of Action
Reviewed Quantity | 100 |
Reason for submission | ok |