QFR No - 8000853049
Defect Details
NC No. 8000853049
NC Date 28/11/2023
NC Submission Date
Part No. S2HT49207B
Part Name OUTER SPRING SILVER- AAGM
Supplier Name & Code 100186-SAGAR SPRINGS PRIVATE LIMITED
ETL Plant 1143-ETL Suspension Halol, Vadodara
Defect Details POWDER COATING NOT OK-RUBBING MARK
 
1. Problem Description
Defect Description RUBBING MARK AND SCRATCH MARK IN AAGM SILVER OUTER SPRING
Detection Stage Inprocess
Problem Severity Aesthetic
NG Quantity 490
Is Defect Repeatative? Yes
Defect Sketch / Photo dhsnflow3mtppp15idcmtd4b.jpg
Supplier Communication Details
Quality Head Email ID quality@sagarsprings.com
Plant Head/CEO Email ID ajai.singh@sagarsprings.com
MD Email ID sagar@sagarsprings.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
1980
0
0
280
0
2260
Check Qty
1980
0
0
280
0
2260
NG Qty
490
0
0
0
0
490
 
Scrap 0
Rework 490
Under Deviation 0
Containment Action
SSPL represntative visited ETL verify the problem and segregated spring at ETL end 490 nos recall to sagar springs and will be recovered
 
3. Process Flow
Process Flow Description
coil-tempring,end grinding-shot pinning-tempring-sq connection Htchecking-pre-treatment-powder coating-inspection-packing-dispatch
 
4. Process Details
Process / Operation Packing
Outsource No
Machine / Cell Packing
Machine / Cell No. 130
5. Problem Analysis
Type Possible Cause Fact Verification Jud
ManPerson negligence on spring handlingFound persons are aware and handling it properlO
MaterialPowder deffectiveFound powder is OK as problem is not 100%O
MethodPacking method is not adequateSpring is packed in box which is tight which result in to rubbing markX
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method Visual inspection
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
7. Root Cause Analysis (Occurance)
Why 1 Rubbing mark on silver spring
Why 2 Spring outer surface is get rubbed hardly
Why 3 Spring is packed in corrugated box with 30 nos honey comb interlock is tight
Why 4 Bin for spring is not available as regular bins area short in height while spring height is more
Why 5
Root Cause (Occurance) Spring pack in corrugated box which is tight and same bin for particular spring is not available
 
Root Cause Analysis (Outflow)
Why 1 Spring with rubbing mark move to customer
Why 2 Rubbing mark generated after packing hence it is not detected
Why 3
Why 4
Why 5
Root Cause (Outflow) Rubbing mark generate after packing in corrugated box
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceBin with proper height with plastic insert will be developed and same will be introduced for packingPowder Coating Supervisor31/12/202328/12/2023Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System No
Change Details As rubbing mark is in packing hence packing mode is change so there is no need in change in inspection method
Inspection Method Other
Other Inspection Method Visual Inspection
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) Earlier springs was dispatched in corrugated box which remain tight and generate black rubbing mark on spring Outer surface
601_Occurance_Before.pdf
Occurance (After) Started packing and dispatch spring in Plastic with PP interlock to avoid rubbing mark
601_Occurance_After.pdf
Outflow (Before) Spring is checked and rubbing mark generates after packing hence it not get detected
601_Outflow_Before.pdf
Outflow (After) One point lesson given to inspector and started sampling checking of packed spring
601_Outflow_After.pdf
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant All powder coated spring with metallic silver paint
 
12. Document Review
Documents ControlPlan, PackingStd
Specify Other Document Packing std
 
13. Effectiveness Of Action
Reviewed Quantity 100
Reason for submission ok