QFR No - 8000866611
Defect Details
NC No. 8000866611
NC Date 12/03/2024
NC Submission Date
Part No. F2FA19033M
Part Name K0PG FORK PIPE MACHINED
Supplier Name & Code 101109-TUBE INVESTMENTS OF INDIA LIMI
ETL Plant 1136-ETL Suspension Sanand
Defect Details DIMN.U/SIZE.-DIM 3+0.1 MM DISTANCE NG
 
1. Problem Description
Defect Description Dim 3+0.1 mm observed 2.80 mm (undersize)
Detection Stage Inprocess
Problem Severity Fitment
NG Quantity 300
Is Defect Repeatative? No
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID anandms@tii.murugappa.com
Plant Head/CEO Email ID girisha@tii.murugappa.com
MD Email ID mukeshahuja@tii.murugappa.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
3000
0
0
1000
500
4500
Check Qty
3000
0
0
1000
500
4500
NG Qty
300
0
0
0
0
300
 
Scrap 300
Rework 0
Under Deviation 0
Containment Action
material Checked 100 % for Defective Parameter with Identification Marking
 
3. Process Flow
Process Flow Description
Raw Inward Inspection - CNC Machining - Drilling Operation - Deburring Operation - Oiling - Final Inspection - PDIR - Dispatch.
 
4. Process Details
Process / Operation CNC Machining
Outsource No
Machine / Cell cell No -6
Machine / Cell No. Cell No -6
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MaterialRaw Material ID UndersizeVerified Records & No Issue with Raw tube ID issue foundO
Manoperator SkillVerified through Gemba observation and found Operator Skill with Minimum Level as per MatrixX
MachineMore offset limitChecked In Machine Parameter & found ware offset limit to 0.3 mmX
ToolTool DamageVerified through Simulation and found that ID mark/scoring mark generatedO
 
6. Inspection Method Analysis (Current)
Inspection Method Instrument
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size PDIR
7. Root Cause Analysis (Occurance)
Why 1 Dim. 3+0.1 distance u/s found at customer end
Why 2 ID Chamfer Length 1 mm observed 0.80 mm
Why 3 Total ID Depth found shift in Z –axis in CNC machining
Why 4 Excess offset of 0.2 mm given in Z-axis in CNC machining
Why 5 Manual error in offset Input against 0.02 mm given 0.2 mm.
Root Cause (Occurance) Simen based control CNC M/c ware offset Limit is 0.3 mm.
 
Root Cause Analysis (Outflow)
Why 1 Dim. 3+0.1 distance u/s found at customer end
Why 2 ID Chamfer Length 1 mm observed 0.80 mm
Why 3 Total ID Depth found shift in Z –axis in CNC machining
Why 4 Not detected during final inspection
Why 5 Inspection done as per sampling plan
Root Cause (Outflow) Inspection was done on sampling basis.
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccurancePoint added in Hourly inspection for Inspection with Vernier for Dim 3 mm.& range Define for Vernier InspectionMR. Abishak Yadav12/04/202412/04/2024Completed
OccuranceDiscussed with Simen Controller Manufactures for reduced ware offset limit , denied to change , Training given to Supervisor & operators for offset giving & need to check part for 3 mm dim after every offset given in Z-axis.Mr. Palak Shah13/04/202412/04/2024Completed
OutflowInspection Point added in Final Inspection for Visual Inspection with Master OK & NG Part Displayed at Inspection Table.Mr. Abishek Yadav13/04/202412/04/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details 100% Visual Inspection at final Inspection with compare with OK & NG Part.
Inspection Method Other
Other Inspection Method Visual Inspection
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100 %
10. Evidance of Countermeasure
Occurance (Before) Hourly inspection for Inspection with Vernier for Dim 3 mm.& NO range Define for Vernier Inspection
711_Occurance_Before.pptx
Occurance (After) Hourly inspection for Inspection with Vernier for Dim 3 mm.& range Define for Vernier Inspection
711_Occurance_After.pptx
Outflow (Before) No Inspection Point added in Final Inspection for Visual Inspection & No Defect Samples Displayed
711_Outflow_Before.pptx
Outflow (After) Inspection Point added in Final Inspection for Visual Inspection & Defect Samples Displayed
711_Outflow_After.pptx
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant K86 -A
 
12. Document Review
Documents InspCheckSheet
Specify Other Document NO
 
13. Effectiveness Of Action
Reviewed Quantity 5
Reason for submission DIMN.U/SIZE.-DIM 3+0.1 MM DISTANCE NG.