QFR No - 8000870485
Defect Details
NC No. | 8000870485 |
NC Date | 08/04/2024 |
NC Submission Date | |
Part No. | 520BK01573 |
Part Name | CALIPER BODY INTEGRAL TYPE PULSAR |
Supplier Name & Code | 101414-G. S. ENGINEERING |
ETL Plant | 1120-ETL K-226/2 Disc Brakes |
Defect Details | BLOW HOLES-PIN HOLE, BLOW HOLE DENT &DAMAGED |
1. Problem Description
Defect Description | BLOW HOLES-PIN HOLE, BLOW HOLE DENT &DAMAGED |
Detection Stage | Receipt |
Problem Severity | Aesthetic |
NG Quantity | 600 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | bhange.shrikant@rediffmail.com |
Plant Head/CEO Email ID | subhashmarathe45@gmail.com |
MD Email ID |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
4780
|
0
|
0
|
0
|
0
|
4780
|
Check Qty |
4780
|
0
|
0
|
0
|
0
|
4780
|
NG Qty |
600
|
0
|
0
|
0
|
0
|
600
|
Scrap | 600 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
Segregation to ETL end |
3. Process Flow
Process Flow Description |
---|
Raw material -- Melting -- Degassing -- Core manufacturing -- Casting manufacturing -- De-coring -- Gate cutting -- Fettling & Buffing -- Punching -- Heat Treatment -- Shot Blassting -- Finel Inspection -- Dispatch. |
4. Process Details
Process / Operation | GDC |
Outsource | No |
Machine / Cell | GDC Machine |
Machine / Cell No. | M/C No.:- 03 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Man | Turbulence is created while pouring metal into the die | Saucer is arranged for pouring the metal so that the metal reaches all the cavities uniformly | O |
Tool | Insufficient air vents in the die, core gas was entrapment | Adequate air vents are provided in the die so that air escapes easily | O |
6. Inspection Method Analysis (Current)
Inspection Method | Other |
Other Inspection Method | Visualy |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100 % |
7. Root Cause Analysis (Occurance)
Why 1 | Blow hole observed in casting |
Why 2 | core gas entrapped in casting during process |
Why 3 | Inadequate venting to escape gas from cavity during casting |
Why 4 | |
Why 5 | |
Root Cause (Occurance) | Inadequate venting to escape gas from cavity during casting |
Root Cause Analysis (Outflow)
Why 1 | Blow hole observed in casting |
Why 2 | Visually not detected in casting |
Why 3 | Open after machining process at customer end |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | Open after machining process at customer end |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Outflow | Training given to operator & Q gate inspector. 100% inspection before & after shot blasting | Mr. S Dhabe | 06/05/2024 | 29/04/2024 | Completed |
Occurance | Vent to be provided in die from easy escape of gases during casting | Mr. S Marathe | 06/05/2024 | 29/04/2024 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | in-process every hour a visual inspection by production supervisor / QA, DP test is conducted every shift ,100% visual inspection before & after shot blasting & 100% visual inspection before final dispatch. |
Inspection Method | Other |
Other Inspection Method | Visually |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
10. Evidance of Countermeasure
Occurance (Before) |
Air vents depth 0.1mm .Inadequate air passing through this 739_Occurance_Before.jpg |
Occurance (After) |
Air vents depth 0.2mm. This helps the air to escape freely 739_Occurance_After.jpg |
Outflow (Before) |
Eye sequence chart 739_Outflow_Before.pdf |
Outflow (After) |
Eye sequence chart is updated 739_Outflow_After.pdf |
11. Horizontal Deployment
Horizontal Deployment Required | No |
Applicable Machine / Model / Plant | GDC |
12. Document Review
Documents | WISOP |
Specify Other Document | NO |
13. Effectiveness Of Action
Reviewed Quantity | 200 |
Reason for submission | No defect observed in latest lot |