QFR No - 8000870485
Defect Details
NC No. 8000870485
NC Date 08/04/2024
NC Submission Date
Part No. 520BK01573
Part Name CALIPER BODY INTEGRAL TYPE PULSAR
Supplier Name & Code 101414-G. S. ENGINEERING
ETL Plant 1120-ETL K-226/2 Disc Brakes
Defect Details BLOW HOLES-PIN HOLE, BLOW HOLE DENT &DAMAGED
 
1. Problem Description
Defect Description BLOW HOLES-PIN HOLE, BLOW HOLE DENT &DAMAGED
Detection Stage Receipt
Problem Severity Aesthetic
NG Quantity 600
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID bhange.shrikant@rediffmail.com
Plant Head/CEO Email ID subhashmarathe45@gmail.com
MD Email ID
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
4780
0
0
0
0
4780
Check Qty
4780
0
0
0
0
4780
NG Qty
600
0
0
0
0
600
 
Scrap 600
Rework 0
Under Deviation 0
Containment Action
Segregation to ETL end
 
3. Process Flow
Process Flow Description
Raw material -- Melting -- Degassing -- Core manufacturing -- Casting manufacturing -- De-coring -- Gate cutting -- Fettling & Buffing -- Punching -- Heat Treatment -- Shot Blassting -- Finel Inspection -- Dispatch.
 
4. Process Details
Process / Operation GDC
Outsource No
Machine / Cell GDC Machine
Machine / Cell No. M/C No.:- 03
5. Problem Analysis
Type Possible Cause Fact Verification Jud
ManTurbulence is created while pouring metal into the dieSaucer is arranged for pouring the metal so that the metal reaches all the cavities uniformlyO
ToolInsufficient air vents in the die, core gas was entrapmentAdequate air vents are provided in the die so that air escapes easilyO
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method Visualy
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100 %
7. Root Cause Analysis (Occurance)
Why 1 Blow hole observed in casting
Why 2 core gas entrapped in casting during process
Why 3 Inadequate venting to escape gas from cavity during casting
Why 4
Why 5
Root Cause (Occurance) Inadequate venting to escape gas from cavity during casting
 
Root Cause Analysis (Outflow)
Why 1 Blow hole observed in casting
Why 2 Visually not detected in casting
Why 3 Open after machining process at customer end
Why 4
Why 5
Root Cause (Outflow) Open after machining process at customer end
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OutflowTraining given to operator & Q gate inspector. 100% inspection before & after shot blastingMr. S Dhabe06/05/202429/04/2024Completed
OccuranceVent to be provided in die from easy escape of gases during castingMr. S Marathe06/05/202429/04/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details in-process every hour a visual inspection by production supervisor / QA, DP test is conducted every shift ,100% visual inspection before & after shot blasting & 100% visual inspection before final dispatch.
Inspection Method Other
Other Inspection Method Visually
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) Air vents depth 0.1mm .Inadequate air passing through this
739_Occurance_Before.jpg
Occurance (After) Air vents depth 0.2mm. This helps the air to escape freely
739_Occurance_After.jpg
Outflow (Before) Eye sequence chart
739_Outflow_Before.pdf
Outflow (After) Eye sequence chart is updated
739_Outflow_After.pdf
 
11. Horizontal Deployment
Horizontal Deployment Required No
Applicable Machine / Model / Plant GDC
 
12. Document Review
Documents WISOP
Specify Other Document NO
 
13. Effectiveness Of Action
Reviewed Quantity 200
Reason for submission No defect observed in latest lot