QFR No - 8000874506
Defect Details
NC No. | 8000874506 |
NC Date | 16/05/2024 |
NC Submission Date | |
Part No. | 520DZ00212 |
Part Name | FORK BOLT K60-(DS181012) |
Supplier Name & Code | 100189-SANGKAJ STEEL PVT LTD. |
ETL Plant | 1117-ETL K-228/9 Suspension |
Defect Details | NOT AS PER SPECIFICATION-DIMN. 7.5 UNDERSIZE - (4.0+0.1) + (3.5 ) |
1. Problem Description
Defect Description | DIMN. 7.5 UNDERSIZE - (4.0+0.1) + (3.5 ) |
Detection Stage | Inprocess |
Problem Severity | Fitment |
NG Quantity | 402 |
Is Defect Repeatative? | No |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | qualityassurance@sangkaj.com |
Plant Head/CEO Email ID | steel@sangkaj.com |
MD Email ID | anirudh.2007@hotmail.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
1600
|
0
|
0
|
800
|
1000
|
3400
|
Check Qty |
1600
|
0
|
0
|
800
|
1000
|
3400
|
NG Qty |
402
|
0
|
0
|
36
|
0
|
438
|
Scrap | 436 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
All material at ETL End & at Sangkaj Steel is segregated, Defective Qty is scrapped. |
3. Process Flow
Process Flow Description |
---|
RM Inward-RM Inward inspection-Traub Machining(Semi-finish Blank)-Grinding-Tapping-Thread Rolling-Plating-Final Inspection-Packing & dispatch |
4. Process Details
Process / Operation | Traub Machining |
Outsource | Yes |
Machine / Cell | Traub machine |
Machine / Cell No. | 04 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Tool | Tool Worn Out | Worn Out Tool Doesn`t Cause huge Variation | X |
Man | New or Unskilled operator | Experienced & Skilled Operator is deputed for production | X |
Material | Input Material not ok | Part manufactured through Continuous bar Feeding & RM Bar Found OK | X |
Method | Inadequate Inspection Method | No Checkpoint for the Parameter in the Inprocess & in Final Inspection. | O |
Machine | Variation due to Machine | Machine Condition found ok | X |
Tool | Wrong Tool Used | part produced by using another tool used for similar category Parts | O |
6. Inspection Method Analysis (Current)
Inspection Method | Instrument |
Other Inspection Method | |
Check Point at Final Inspection | No |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 50:500 |
7. Root Cause Analysis (Occurance)
Why 1 | 7.50 mm Dimension found undersize |
Why 2 | Wrong forming Tool used for machining |
Why 3 | Forming Tools not identified with Part Names. |
Why 4 | Tool Identification not mentioned in the WI |
Why 5 | |
Root Cause (Occurance) | Tool Identification not mentioned in the WI |
Root Cause Analysis (Outflow)
Why 1 | 7.50 mm Dimension found undersize |
Why 2 | Defective Parts Skipped from Inspection. |
Why 3 | During Inspection this parameter is not checked |
Why 4 | Verification of this parameter not Included in Inspection Checklists. |
Why 5 | Inspection Checklists are inadequate. |
Root Cause (Outflow) | Inspection Checklists are Inadequate |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Outflow | 7.50mm Dimension Verification added in Following Checklists- 1. Supplier In-process Inspection Report, 2.Supplier PDIR Report, 3.Sangkaj Steel`s Inward Inspection Report 4.PDIR | Mr. Anil Chaudhari | 03/06/2024 | 03/06/2024 | Completed |
Occurance | 1.Forming Tools are identified with Part names. 2.Setting WI Updated, it is mentioned in the WI that Every Tool should have Part Names on them. | Mr. Anil Chaudhari | 03/06/2024 | 03/06/2024 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | Dimension 3.50mm Added In Supplier PDIR, Supplier In-process Inspection Report, Inward Inspection & PDI Report of Sangkaj Steel. Inspection will be Followed on Sampling Basis. |
Inspection Method | Instrument |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 50:500 |
10. Evidance of Countermeasure
Occurance (Before) |
No Identification of Forming Tool with part Names 809_Occurance_Before.pptx |
Occurance (After) |
Part Names Engraved on the Tool with manual Engraving Machine 809_Occurance_After.pptx |
Outflow (Before) |
No Checkpoint Available for this Dimension 809_Outflow_Before.pptx |
Outflow (After) |
Checkpoint added in the PDIR, Hourly inspection and Inward Inspection Report 809_Outflow_After.pptx |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | Fork Bolt JD, 5TSF |
12. Document Review
Documents | ControlPlan, InspCheckSheet |
Specify Other Document | PDIR |
13. Effectiveness Of Action
Reviewed Quantity | 50 |
Reason for submission | Judgment wrong Occurrence side root cause can do better |