QFR No - 8000879355
Defect Details
NC No. 8000879355
NC Date 22/06/2024
NC Submission Date
Part No. F2DZ04603B
Part Name FORK BOLT J1A & J1D
Supplier Name & Code 100189-SANGKAJ STEEL PVT LTD.
ETL Plant 1117-ETL K-228/9 Suspension
Defect Details THREADING NOT OK-M10 THREAD MISSING
 
1. Problem Description
Defect Description M10 THREAD MISSING
Detection Stage Inprocess
Problem Severity Fitment
NG Quantity 1
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID qualityassurance@sangkaj.com
Plant Head/CEO Email ID steel@sangkaj.com
MD Email ID anirudh.2007@hotmail.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
384
0
0
816
0
1200
Check Qty
384
0
0
816
0
1200
NG Qty
0
0
0
0
0
0
 
Scrap 0
Rework 0
Under Deviation 0
Containment Action
Segregation of the Available stock at Customer End done. Rechecking of RF Material Completed.
 
3. Process Flow
Process Flow Description
RM inward - RM Inward Inspection - S/F Blank (Traub Machining) - CNC turning 1st - CNC Turning 2nd - Milling - Tapping- plating-Final Inspection-Packing & Dispatch
 
4. Process Details
Process / Operation Tapping
Outsource No
Machine / Cell Tapping Cell
Machine / Cell No. 03
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MethodInadequate Inspection methodSampling Inspection of M10 Threads is done along with 100% Visual InspectionX
MethodOperation finished & unfinished parts Mix-upOperator observed keeping both operation done & remained parts on machineX
ToolTap Worn OutTap Condition Verified, Found OkO
MaterialInput Material Drill ID OversizeDrill ID found ok, Specified 8.50+0.1, observed 8.58mmO
MachineStroke length set lessfixed c-type Stopper has been installed between the two Dodge to Set Tapping lengthO
ManUnskilled operatorSkilled Operator Deployed on Machine, Skill Level L2, Verified Skill matrix, Found OkO
 
6. Inspection Method Analysis (Current)
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 05 Nos
7. Root Cause Analysis (Occurance)
Why 1 Part Without Threads found at Customer end
Why 2 Without operation part mixed up with finished part on machine
Why 3 Both operation Finished & unfinished parts are kept on Machine.
Why 4 Operator not Followed the Standard Work instruction.
Why 5
Root Cause (Occurance) Operator not Followed Standard Work Instruction.
 
Root Cause Analysis (Outflow)
Why 1 Part Without Threads found at Customer end
Why 2 Operation missing part Skipped from Final Inspection
Why 3 Sampling Inspection done for threading with TPG
Why 4 Inadequate sample size during Final inspection
Why 5
Root Cause (Outflow) Inadequate sample size during Final inspection
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
Outflow1. Sample size Increased for Inspection with TPG & 100% Inspection with M10 thread Minor Dia. PPG. Training given to Inspector. Q- Alert Displayed on machine and at Final Inspection.Mr. Anil Chaudhari25/06/202425/06/2024Completed
Occurance1.Training given to operator about the Proper Working Method. 2.Output bin Kept within reach of operator near machine.Mr. Santosh Raut25/06/202425/06/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details 100% Inspection of threading Minor Diameter with no-Go PPG along with visual inspection. Without operation parts will get Detected by PPG.
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) operator kept both input And output material on Machine
884_Occurance_Before.pptx
Occurance (After) Training given to operator to Follow the Work Instruction and keep input /output material Separately to avoid the Chances of mixup.
884_Occurance_After.pptx
Outflow (Before) 100% Visual Inspection & Sampling Inspection done with TPG
884_Outflow_Before.pptx
Outflow (After) 100% Inspection with threading minor Diameter PPG to Detect the operation missing part.
884_Outflow_After.pptx
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant All Fork Bolt
 
12. Document Review
Documents ControlPlan, InspCheckSheet
Specify Other Document Inspection Standard
 
13. Effectiveness Of Action
Reviewed Quantity 250
Reason for submission OK