QFR No - 8000879789
Defect Details
NC No. 8000879789
NC Date 25/06/2024
NC Submission Date
Part No. 550KH03002
Part Name REBOUND SPRING-PRFH-006
Supplier Name & Code 101245-SAGAR SPRINGS PVT LTD
ETL Plant 1146-ETL Suspension Narasapura
Defect Details BEND-
 
1. Problem Description
Defect Description Rebound Spring bend issue .
Detection Stage Inprocess
Problem Severity Fitment
NG Quantity 2
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID quality@sagarsprings.com
Plant Head/CEO Email ID sagarsprings@gmail.com
MD Email ID
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
15000
0
0
5000
0
20000
Check Qty
15000
0
0
5000
0
20000
NG Qty
2
0
0
0
0
2
 
Scrap 2
Rework 0
Under Deviation 0
Containment Action
Scrap
 
3. Process Flow
Process Flow Description
Coiling - Tempering - Grinding - Shot Peening - Tempering - Oiling - Packing
 
4. Process Details
Process / Operation Material Handling / Movement between operations
Outsource No
Machine / Cell Material Handling / Movement between operations
Machine / Cell No. Trolley
5. Problem Analysis
Type Possible Cause Fact Verification Jud
ManUntrained operatorTrained operators working at all process stagesO
MethodSpring bend during material handlingMaterial handled / moved in trolleys and potential chances of bendX
ManNew operatorExperienced operators working at all process atagesO
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method Sampling inspection
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size sample pla
7. Root Cause Analysis (Occurance)
Why 1 Spring bend during material handling
Why 2 Material handling in trolleys caused bend
Why 3 During material unloading springs fallen on ground and trolly wheel passed on spring and same springs got mixed up with lot
Why 4 Material handling trolley design constrain
Why 5
Root Cause (Occurance) Material handling trolley design constrain
 
Root Cause Analysis (Outflow)
Why 1 Spring Bend
Why 2 Spring bend problem could not able to detect at final inspection
Why 3 Sampling inspection
Why 4
Why 5
Root Cause (Outflow) Sampling inspection
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceNew model trolley designed to handle / move rebound springs to prevent bendSSPL30/06/202430/06/2024Completed
OutflowVisual inspection will be done after final inspection for free from bend & before oiling and packingSSPL30/06/202430/06/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details Visual Inspection
Inspection Method Other
Other Inspection Method Visual Inspection
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100% Visua
10. Evidance of Countermeasure
Occurance (Before) Material handling trolley design constraint causing spring bend during unloading springs
886_Occurance_Before.pptx
Occurance (After) Trolley design modified to prevent spring bend issue
886_Occurance_After.pptx
Outflow (Before) At final Inspection sampling inspection followed caused non detection of spring bend
886_Outflow_Before.pptx
Outflow (After) After final inspection visual inspection before coiling to detect spring bend issue
886_Outflow_After.pptx
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant Action applicable for all rebound springs
 
12. Document Review
Documents PFMEA
Specify Other Document OPL
 
13. Effectiveness Of Action
Reviewed Quantity 10000
Reason for submission Reviewed next two lots found ok no issue .