QFR No - 8000881302
Defect Details
NC No. | 8000881302 |
NC Date | 05/07/2024 |
NC Submission Date | |
Part No. | B2BK05603O |
Part Name | CALIPER BODY RAW-N-TORQ CBS |
Supplier Name & Code | 100398-MANOJ INDUSTRIES |
ETL Plant | 1120-ETL K-226/2 Disc Brakes |
Defect Details | BLOW HOLES-BLOW HOLE, DENT DAMAGE |
1. Problem Description
Defect Description | EXTRA CASTING IN PAD SPRING AREA, BH & DAMAGED |
Detection Stage | Inprocess |
Problem Severity | Fitment |
NG Quantity | 316 |
Is Defect Repeatative? | No |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | dlad@manojind.com |
Plant Head/CEO Email ID | siju@manojind.com |
MD Email ID | mgnt@manojindustrieskop.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
7646
|
300
|
0
|
0
|
1200
|
9146
|
Check Qty |
7646
|
300
|
0
|
0
|
1200
|
9146
|
NG Qty |
316
|
0
|
0
|
0
|
0
|
316
|
Scrap | 316 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
Sort out all pipe line material |
3. Process Flow
Process Flow Description |
---|
-- |
4. Process Details
Process / Operation | Casting production |
Outsource | No |
Machine / Cell | MI Tilt -9 |
Machine / Cell No. | - |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Material | Sand core finish rough at pad spring area | Visually verified sand core | O |
6. Inspection Method Analysis (Current)
Inspection Method | Other |
Other Inspection Method | Visually |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
7. Root Cause Analysis (Occurance)
Why 1 | EXTRA CASTING IN PAD SPRING AREA |
Why 2 | Its sand core area,Due to sand fall casting get extra material |
Why 3 | Sand core observed rough at profile area |
Why 4 | |
Why 5 | |
Root Cause (Occurance) | Sand core observed rough at profile area |
Root Cause Analysis (Outflow)
Why 1 | EXTRA CASTING IN PAD SPRING AREA |
Why 2 | Skipped by final inspection. |
Why 3 | |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | Skipped by final inspection. |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | For smooth & avoid extra material at pad spring area silver paint applied at sand core profile area | Siju D | 09/07/2024 | 09/07/2024 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | After final inspection dot marking done on casting at pad spring area. |
Inspection Method | Other |
Other Inspection Method | Visually |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
10. Evidance of Countermeasure
Occurance (Before) |
Sand core observed rough at pad spring area 904_Occurance_Before.pptx |
Occurance (After) |
Silver paint applied at sand core profile area. 904_Occurance_After.pptx |
Outflow (Before) |
Skipped by final inspection 904_Outflow_Before.pptx |
Outflow (After) |
Q alert displayed at final inspection area 904_Outflow_After.pptx |
11. Horizontal Deployment
Horizontal Deployment Required | No |
Applicable Machine / Model / Plant | -- |
12. Document Review
Documents | |
Specify Other Document | -- |
13. Effectiveness Of Action
Reviewed Quantity | 200 |
Reason for submission | Improvement found in next lots |