QFR No - 8000881358
Defect Details
NC No. | 8000881358 |
NC Date | 05/07/2024 |
NC Submission Date | |
Part No. | B2RC03824O |
Part Name | CALIPER PISTON ANODISED DIA 28 |
Supplier Name & Code | 101261-BHOGALE AUTOMOTIVE PRIVATE LIM |
ETL Plant | 1120-ETL K-226/2 Disc Brakes |
Defect Details | SURFACE FINISH NOT OK-UNCLEAN AT BOTTOM |
1. Problem Description
Defect Description | Unclean AT Bottom Side |
Detection Stage | Receipt |
Problem Severity | Fitment |
NG Quantity | 23 |
Is Defect Repeatative? | No |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | nikhil.kulkarni@bhogaleauto.com |
Plant Head/CEO Email ID | rajendra.randive@bhogaleauto.com |
MD Email ID |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
1000
|
0
|
0
|
1300
|
900
|
3200
|
Check Qty |
1000
|
0
|
0
|
1300
|
900
|
3200
|
NG Qty |
23
|
0
|
0
|
0
|
0
|
23
|
Scrap | 23 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
1) 2300 parts verified in pipeline. 2) 2nd firewall implemented till issue resolved. |
3. Process Flow
Process Flow Description |
---|
Reciept insp. > Forging > Heat treatment > Trimming > Grinding > Final Inspection > Packing and dispatch |
4. Process Details
Process / Operation | Forging |
Outsource | No |
Machine / Cell | Forging press |
Machine / Cell No. | P1 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Man | Die not cleaned | Forging lubrication paste diposited on die in running | O |
Machine | Pressure variation | Checked consistancy over 100 parts, found ok | X |
Material | Short input billet size | Billet cutting is program controlled and checked repeatability found ok | X |
6. Inspection Method Analysis (Current)
Inspection Method | Other |
Other Inspection Method | Manual/ Visual |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 10 |
7. Root Cause Analysis (Occurance)
Why 1 | After CNC machining 2nd, part having unclean face. |
Why 2 | Machining not done on partial outer portion of face. |
Why 3 | Forging face is not having flatness, as required. |
Why 4 | Forging ejection pin having lubrication paste stuck on corners. |
Why 5 | Die and pin does not cleaned, during production. |
Root Cause (Occurance) | Tooling not cleaned frequently during production. |
Root Cause Analysis (Outflow)
Why 1 | Defect skipped from visual inspection. |
Why 2 | Due to surface dying, surface appearance matches with machining |
Why 3 | Difference difficult to understand |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | Inspector not understand the defect |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | Tool cleaning after every 500 nos forging is implemented in WIS | NSK | 28/06/2024 | Pending | |
Occurance | Control plan revised | NSK | 28/06/2024 | Pending | |
Outflow | Refreshment training given to inspectors. | NSK | 27/06/2024 | Pending |
9. Inspection Method After Customer Complaint
Change In Inspection System | No |
Change Details | No change in inspection method |
Inspection Method | Other |
Other Inspection Method | Visual inspection |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | all |
10. Evidance of Countermeasure
Occurance (Before) |
No tool cleaning frequency defined in forging WIS 907_Occurance_Before.png |
Occurance (After) |
Cleaning frequency defined in forging WIS 907_Occurance_After.png |
Outflow (Before) |
Defect forging unclean not in visual inspection WIS 907_Outflow_Before.pdf |
Outflow (After) |
Defect forging unclean added in visual inspection WIS 907_Outflow_After.pdf |
11. Horizontal Deployment
Horizontal Deployment Required | No |
Applicable Machine / Model / Plant | Not applicable |
12. Document Review
Documents | ControlPlan, WISOP |
Specify Other Document | Not applicable |
13. Effectiveness Of Action
Reviewed Quantity | |
Reason for submission |