QFR No - 8000881358
Defect Details
NC No. 8000881358
NC Date 05/07/2024
NC Submission Date
Part No. B2RC03824O
Part Name CALIPER PISTON ANODISED DIA 28
Supplier Name & Code 101261-BHOGALE AUTOMOTIVE PRIVATE LIM
ETL Plant 1120-ETL K-226/2 Disc Brakes
Defect Details SURFACE FINISH NOT OK-UNCLEAN AT BOTTOM
 
1. Problem Description
Defect Description Unclean AT Bottom Side
Detection Stage Receipt
Problem Severity Fitment
NG Quantity 23
Is Defect Repeatative? No
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID nikhil.kulkarni@bhogaleauto.com
Plant Head/CEO Email ID rajendra.randive@bhogaleauto.com
MD Email ID
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
1000
0
0
1300
900
3200
Check Qty
1000
0
0
1300
900
3200
NG Qty
23
0
0
0
0
23
 
Scrap 23
Rework 0
Under Deviation 0
Containment Action
1) 2300 parts verified in pipeline. 2) 2nd firewall implemented till issue resolved.
 
3. Process Flow
Process Flow Description
Reciept insp. > Forging > Heat treatment > Trimming > Grinding > Final Inspection > Packing and dispatch
 
4. Process Details
Process / Operation Forging
Outsource No
Machine / Cell Forging press
Machine / Cell No. P1
5. Problem Analysis
Type Possible Cause Fact Verification Jud
ManDie not cleanedForging lubrication paste diposited on die in runningO
MachinePressure variationChecked consistancy over 100 parts, found okX
MaterialShort input billet sizeBillet cutting is program controlled and checked repeatability found okX
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method Manual/ Visual
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 10
7. Root Cause Analysis (Occurance)
Why 1 After CNC machining 2nd, part having unclean face.
Why 2 Machining not done on partial outer portion of face.
Why 3 Forging face is not having flatness, as required.
Why 4 Forging ejection pin having lubrication paste stuck on corners.
Why 5 Die and pin does not cleaned, during production.
Root Cause (Occurance) Tooling not cleaned frequently during production.
 
Root Cause Analysis (Outflow)
Why 1 Defect skipped from visual inspection.
Why 2 Due to surface dying, surface appearance matches with machining
Why 3 Difference difficult to understand
Why 4
Why 5
Root Cause (Outflow) Inspector not understand the defect
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceTool cleaning after every 500 nos forging is implemented in WISNSK28/06/2024Pending
OccuranceControl plan revisedNSK28/06/2024Pending
OutflowRefreshment training given to inspectors.NSK27/06/2024Pending
 
9. Inspection Method After Customer Complaint
Change In Inspection System No
Change Details No change in inspection method
Inspection Method Other
Other Inspection Method Visual inspection
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size all
10. Evidance of Countermeasure
Occurance (Before) No tool cleaning frequency defined in forging WIS
907_Occurance_Before.png
Occurance (After) Cleaning frequency defined in forging WIS
907_Occurance_After.png
Outflow (Before) Defect forging unclean not in visual inspection WIS
907_Outflow_Before.pdf
Outflow (After) Defect forging unclean added in visual inspection WIS
907_Outflow_After.pdf
 
11. Horizontal Deployment
Horizontal Deployment Required No
Applicable Machine / Model / Plant Not applicable
 
12. Document Review
Documents ControlPlan, WISOP
Specify Other Document Not applicable
 
13. Effectiveness Of Action
Reviewed Quantity
Reason for submission