QFR No - 8000886611
Defect Details
NC No. 8000886611
NC Date 12/08/2024
NC Submission Date
Part No. F2FQ00407B
Part Name HOLDER HANDLE UPPER P/C (XF-521)
Supplier Name & Code 201092-PRANEEL INDUSTRIES
ETL Plant 1117-ETL K-228/9 Suspension
Defect Details B/H INSIDE BORE- BLOW HOLE
 
1. Problem Description
Defect Description Bore ID Blow Hole
Detection Stage Receipt
Problem Severity Aesthetic
NG Quantity 22
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID quality@praneelgroup.com
Plant Head/CEO Email ID praneelindustries@rediiffmail.com
MD Email ID anilpatil@praneelgroup.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
1633
0
0
250
0
1883
Check Qty
1633
0
0
250
0
1883
NG Qty
22
0
0
10
0
32
 
Scrap 32
Rework 0
Under Deviation 0
Containment Action
All material at ETL end and at In-house sagrigated and NG quantity rejected at ETL end and at In-house.
 
3. Process Flow
Process Flow Description
Raw casting inward =>Powder Coating=>Powder Coating inward=>VMC Machining=>De-burring=>Final Inspection=>Packing and Dispatch.
 
4. Process Details
Process / Operation VMC Machining
Outsource No
Machine / Cell VMC Machine
Machine / Cell No. VMC Cell
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MachineMachine parameter not as per control planVerify the machine parameter and found OkO
ToolDrill not as per required.Verify the drill size and found ok.O
MaterialMaterial not as per required specification.Verify the material report found Ok.O
ManSkilled inspector not availableVerify the skill matrix,found Ok.O
MethodInspection method not as per required.Verify the checking method and found inadequate.X
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method Visual
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size samp.plan
7. Root Cause Analysis (Occurance)
Why 1 Blow Hole inside the bore size 8.4+0.1mm.
Why 2 Rubbish metal poured in the die.
Why 3 Impurities observed after degassing in the furnace.
Why 4 Metal cleaning process not done properly.
Why 5
Root Cause (Occurance) Metal cleaning process not done properly.
 
Root Cause Analysis (Outflow)
Why 1 Blow Hole inside the bore size 8.4+0.1mm.
Why 2 Skipped from final inspection.
Why 3 No awareness about checking the blow hole inside the bore.
Why 4
Why 5
Root Cause (Outflow) No awareness about checking the blow hole inside the bore.
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceWire Mesh filter to be implementMr.Ramdas Boinale05/09/202411/09/2024Completed
OutflowAwareness and Training given to inspector for checking blow hole inside the bore.Mr.Yogesh Sonune19/08/202419/08/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details Visual inspection started for Blow Hole inside the bore.
Inspection Method Other
Other Inspection Method Visual inspection
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size samp.plan
10. Evidance of Countermeasure
Occurance (Before) No any wire mesh filter provided at the insert.
1005_Occurance_Before.pptx
Occurance (After) Wire mesh filter will be implement at the insert.
1005_Occurance_After.pptx
Outflow (Before) Before no any marking at bore 8.40+0.1mm.
1005_Outflow_Before.pptx
Outflow (After) After inspection marking started near to the bore 8.40+0.1mm and Training provided for the same.
1005_Outflow_After.pptx
 
11. Horizontal Deployment
Horizontal Deployment Required No
Applicable Machine / Model / Plant --
 
12. Document Review
Documents WISOP
Specify Other Document Training record
 
13. Effectiveness Of Action
Reviewed Quantity 50
Reason for submission OK