QFR No - 8000890800
Defect Details
NC No. | 8000890800 |
NC Date | 12/09/2024 |
NC Submission Date | |
Part No. | F2FA19033M |
Part Name | K0PG FORK PIPE MACHINED |
Supplier Name & Code | 101109-TUBE INVESTMENTS OF INDIA LIMI |
ETL Plant | 1136-ETL Suspension Sanand |
Defect Details | CRACK-HEAVY CRACK PART |
1. Problem Description
Defect Description | Fork pipe K0PG crack problem. |
Detection Stage | Inprocess |
Problem Severity | Function |
NG Quantity | 1 |
Is Defect Repeatative? | No |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | anandms@tii.murugappa.com |
Plant Head/CEO Email ID | girisha@tii.murugappa.com |
MD Email ID | mukeshahuja@tii.murugappa.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
5000
|
0
|
0
|
1500
|
67000
|
73500
|
Check Qty |
5000
|
0
|
0
|
1500
|
12000
|
18500
|
NG Qty |
4
|
0
|
0
|
0
|
0
|
4
|
Scrap | 4 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
100 % Visual inspection done for all available material at ETL after Grinding & will continue for next 1 week. & 100% Visual Inspection stated after machining operation for all available Raw material stock before dispatch to ETL. |
3. Process Flow
Process Flow Description |
---|
TUBE FORMING - ANNEALING - WET PROCESS - PUSH POINTING - DRAWING - STRESS RELIEVING - STRAIGHTENING - ECT - CTL - FACING & CHAMFERING - FINAL INSPECTION - PACKING - DISPATCH TO SANAND W/H - INWARD - CNC MACHINING - DRILLING - DIBURRING - FINAL INSPECTION - PACKING - DISPATCH TO ETL. |
4. Process Details
Process / Operation | Tube FORMING |
Outsource | No |
Machine / Cell | --- |
Machine / Cell No. | --- |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Method | Impeder damage | Auto mode paper filter mechanism monitoring every day through IMI Check list. | O |
Method | Insufficient Argon gas flow | Inter lock available for detection alarm if in case of variation in argon flow. | O |
Method | Fin blade broken | As Per report found Seam guide fin blades are broken while thickness change over. | X |
Machine | Less power during start of mill | Auto paint spray unit mechnaism ( 1st Part - NG Paint spray) monitoring through IMI Check | O |
6. Inspection Method Analysis (Current)
Inspection Method | Other |
Other Inspection Method | Eddy Current Testing |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
7. Root Cause Analysis (Occurance)
Why 1 | Tube Crack found at customer end after grinding operation. |
Why 2 | Paste weld at localized area . |
Why 3 | 18th pass fin blade broken as Excess load act on blade side face |
Why 4 | Small weld bead material hit on the fin blade while wall thickness change over. |
Why 5 | Insufficient grinding of end weld joint edges with the current practice. |
Root Cause (Occurance) | Insufficient grinding of end weld joint edges with the current practice. |
Root Cause Analysis (Outflow)
Why 1 | Tube Crack found at customer end after grinding operation. |
Why 2 | Crack occurred after grinding process load |
Why 3 | Paste weld at localized area & it is not detected. |
Why 4 | Eddy current testing m/c is not capture the defect. |
Why 5 | |
Root Cause (Outflow) | Eddy current testing m/c is not capture the defect. |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | Concave c-shape grinding to be done on both edge up to 2 mm from strip width(Grinding strip width allowance: 130 mm to 132 mm). | Mr. Satish | 15/10/2024 | 10/10/2024 | Completed |
Occurance | The end weld ground strip to be verified snap gauge for each end weld period. | Mr. Satish | 15/10/2024 | 10/10/2024 | Completed |
Outflow | ECT setting threshold limit changed from 50% to 40% for stringent control | Mr. Satish | 15/10/2024 | 10/10/2024 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | No |
Change Details | ECT setting threshold limit changed from 50% to 40% for stringent control |
Inspection Method | Other |
Other Inspection Method | Eddy current testing |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
10. Evidance of Countermeasure
Occurance (Before) |
1.Fine edge bead projection even after flat grinding of end weld joint.
2. Visual inspection after every end weld grinding 1089_Occurance_Before.pptx |
Occurance (After) |
1.Concave c-shape grinding to be done on both edge up to 2 mm from strip width.
2.The end weld ground strip to be verified snap gauge for each end weld period. 1089_Occurance_After.pptx |
Outflow (Before) |
Eddy current test threshold setting of upper & lower controlled with 50% 1089_Outflow_Before.pptx |
Outflow (After) |
ECT setting threshold limit changed from 50% to 40% for stringent control 1089_Outflow_After.pptx |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | ALL TFF SIZES. |
12. Document Review
Documents | WISOP |
Specify Other Document | NO |
13. Effectiveness Of Action
Reviewed Quantity | |
Reason for submission |