QFR No - 8000890800
Defect Details
NC No. 8000890800
NC Date 12/09/2024
NC Submission Date
Part No. F2FA19033M
Part Name K0PG FORK PIPE MACHINED
Supplier Name & Code 101109-TUBE INVESTMENTS OF INDIA LIMI
ETL Plant 1136-ETL Suspension Sanand
Defect Details CRACK-HEAVY CRACK PART
 
1. Problem Description
Defect Description Fork pipe K0PG crack problem.
Detection Stage Inprocess
Problem Severity Function
NG Quantity 1
Is Defect Repeatative? No
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID anandms@tii.murugappa.com
Plant Head/CEO Email ID girisha@tii.murugappa.com
MD Email ID mukeshahuja@tii.murugappa.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
5000
0
0
1500
67000
73500
Check Qty
5000
0
0
1500
12000
18500
NG Qty
4
0
0
0
0
4
 
Scrap 4
Rework 0
Under Deviation 0
Containment Action
100 % Visual inspection done for all available material at ETL after Grinding & will continue for next 1 week. & 100% Visual Inspection stated after machining operation for all available Raw material stock before dispatch to ETL.
 
3. Process Flow
Process Flow Description
TUBE FORMING - ANNEALING - WET PROCESS - PUSH POINTING - DRAWING - STRESS RELIEVING - STRAIGHTENING - ECT - CTL - FACING & CHAMFERING - FINAL INSPECTION - PACKING - DISPATCH TO SANAND W/H - INWARD - CNC MACHINING - DRILLING - DIBURRING - FINAL INSPECTION - PACKING - DISPATCH TO ETL.
 
4. Process Details
Process / Operation Tube FORMING
Outsource No
Machine / Cell ---
Machine / Cell No. ---
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MethodImpeder damageAuto mode paper filter mechanism monitoring every day through IMI Check list.O
MethodInsufficient Argon gas flowInter lock available for detection alarm if in case of variation in argon flow.O
MethodFin blade brokenAs Per report found Seam guide fin blades are broken while thickness change over.X
MachineLess power during start of millAuto paint spray unit mechnaism ( 1st Part - NG Paint spray) monitoring through IMI CheckO
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method Eddy Current Testing
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
7. Root Cause Analysis (Occurance)
Why 1 Tube Crack found at customer end after grinding operation.
Why 2 Paste weld at localized area .
Why 3 18th pass fin blade broken as Excess load act on blade side face
Why 4 Small weld bead material hit on the fin blade while wall thickness change over.
Why 5 Insufficient grinding of end weld joint edges with the current practice.
Root Cause (Occurance) Insufficient grinding of end weld joint edges with the current practice.
 
Root Cause Analysis (Outflow)
Why 1 Tube Crack found at customer end after grinding operation.
Why 2 Crack occurred after grinding process load
Why 3 Paste weld at localized area & it is not detected.
Why 4 Eddy current testing m/c is not capture the defect.
Why 5
Root Cause (Outflow) Eddy current testing m/c is not capture the defect.
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceConcave c-shape grinding to be done on both edge up to 2 mm from strip width(Grinding strip width allowance: 130 mm to 132 mm).Mr. Satish15/10/202410/10/2024Completed
OccuranceThe end weld ground strip to be verified snap gauge for each end weld period.Mr. Satish15/10/202410/10/2024Completed
OutflowECT setting threshold limit changed from 50% to 40% for stringent controlMr. Satish15/10/202410/10/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System No
Change Details ECT setting threshold limit changed from 50% to 40% for stringent control
Inspection Method Other
Other Inspection Method Eddy current testing
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) 1.Fine edge bead projection even after flat grinding of end weld joint. 2. Visual inspection after every end weld grinding
1089_Occurance_Before.pptx
Occurance (After) 1.Concave c-shape grinding to be done on both edge up to 2 mm from strip width. 2.The end weld ground strip to be verified snap gauge for each end weld period.
1089_Occurance_After.pptx
Outflow (Before) Eddy current test threshold setting of upper & lower controlled with 50%
1089_Outflow_Before.pptx
Outflow (After) ECT setting threshold limit changed from 50% to 40% for stringent control
1089_Outflow_After.pptx
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant ALL TFF SIZES.
 
12. Document Review
Documents WISOP
Specify Other Document NO
 
13. Effectiveness Of Action
Reviewed Quantity
Reason for submission