QFR No - 7001019734
Defect Details
NC No. | 7001019734 |
NC Date | 01/06/2024 |
NC Submission Date | |
Part No. | F2PH00902B |
Part Name | VALVE RETAINER (C101B) |
Supplier Name & Code | 100106-SHARP ENGINEERS. |
ETL Plant | 1136-ETL Suspension Sanand |
Defect Details | HIGHT U/SIZE.-Total Width undersize |
1. Problem Description
Defect Description | Total width undersize, Specification 9.3 mm observation 8.75 mm |
Detection Stage | Receipt |
Problem Severity | Fitment |
NG Quantity | 4670 |
Is Defect Repeatative? | No |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | quality@apw3.co.in |
Plant Head/CEO Email ID | kurund.ma@sharp-engineers.com |
MD Email ID | urkhandelwal@sharp-engineers.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
10000
|
0
|
5000
|
0
|
10000
|
25000
|
Check Qty |
10000
|
0
|
5000
|
0
|
10000
|
25000
|
NG Qty |
4670
|
0
|
0
|
0
|
0
|
4670
|
Scrap | 4670 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
Segregation done for all the suspected material of pipeline and defective part removed from OK part and quarantine. |
3. Process Flow
Process Flow Description |
---|
10) RM inward 20) RM Storage 30) Parting 40) CNC 1st set up 50) OD grinding 60) Plating (Outsource) 70) Inward Inspection 80) Final inspection 90) Pr-dispatch inspection 100) Packing & forwarding. |
4. Process Details
Process / Operation | CNC Machining |
Outsource | No |
Machine / Cell | Machine Shop |
Machine / Cell No. | SE/CNC 01 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Man | Unskilled manpower | Skilled manpower available | O |
Tool | Tool/Insert worn out | Tool life monitoring as per defined frequency available in the machine interlock. | O |
Machine | Machine Variation | JH/PM as per defined frequency | O |
Material | Suspected NG part in the pipeline material | Pipeline material was NG and not recalled after receipt of customer complaint | X |
Method | Incorrect checking method | common method for inspection by attribute type height gauge | O |
6. Inspection Method Analysis (Current)
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 1:1 |
7. Root Cause Analysis (Occurance)
Why 1 | Total length under part reached at ETL |
Why 2 | NG material of pipeline not recalled |
Why 3 | Because of line stoppage |
Why 4 | |
Why 5 | |
Root Cause (Occurance) | NG material of pipeline not recalled |
Root Cause Analysis (Outflow)
Why 1 | Total length under part reached at ETL |
Why 2 | not detected in the final inspection |
Why 3 | Taper observed at one side of the parts |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | Taper observed at one side of the parts |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | Inventory level of ware house for VALVE RETAINER increase as per defined scheduled qty | Mr. Kurund M.A. | 20/06/2024 | 20/06/2024 | Completed |
Outflow | Part are being checked at both side of the part by attribute type height gauge 100% before dispatch. inspector identification tag are being provided for traceability purpose | Mr. Shaikh L.N | 20/06/2024 | 20/06/2024 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | Component are being checked at both side of the part by attribute type height gauge 100% before dispatch. |
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 1:1 |
10. Evidance of Countermeasure
Occurance (Before) |
NG material of pipeline not recalled because of less material inventory level at warehouse. 833_Occurance_Before.pptx |
Occurance (After) |
Inventory level of ware house for VALVE RETAINER increase as per defined scheduled qty. 833_Occurance_After.xlsx |
Outflow (Before) |
Taper observed at one side of the parts, inspection done only one side of the part. 833_Outflow_Before.pptx |
Outflow (After) |
Part are being checked at both side of the part by attribute type height gauge 100% before dispatch. inspector identification tag are being provided for traceability purpose 833_Outflow_After.pptx |
11. Horizontal Deployment
Horizontal Deployment Required | No |
Applicable Machine / Model / Plant | NA |
12. Document Review
Documents | ControlPlan, PFMEA, WISOP, InspCheckSheet |
Specify Other Document | NA |
13. Effectiveness Of Action
Reviewed Quantity | 5 |
Reason for submission | Total width undersize |