QFR No - 7001062684
Defect Details
NC No. | 7001062684 |
NC Date | 11/10/2024 |
NC Submission Date | |
Part No. | 530BU00302 |
Part Name | Stricker Cap |
Supplier Name & Code | 100144-AURANGABAD PRESSINGS |
ETL Plant | 1118-ETL E-92,93 Suspension |
Defect Details | DIMETER UNDERSIZE-I/D U/SIZE SPE=43.60-0.30 GAUGE NOT PASS |
1. Problem Description
Defect Description | DIMETER UNDERSIZE-I/D U/SIZE SPE=43.60-0.30 GAUGE NOT PASS |
Detection Stage | Receipt |
Problem Severity | Fitment |
NG Quantity | 900 |
Is Defect Repeatative? | No |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | quality@apw3.co.in |
Plant Head/CEO Email ID | aurangabadpressings@apw3.co.in |
MD Email ID | shashikant@apw3.co.in |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
5139
|
0
|
0
|
0
|
2500
|
7639
|
Check Qty |
5139
|
0
|
0
|
0
|
2500
|
7639
|
NG Qty |
2511
|
0
|
0
|
0
|
1100
|
3611
|
Scrap | 0 |
Rework | 1700 |
Under Deviation | 0 |
Containment Action |
---|
Segregation all material |
3. Process Flow
Process Flow Description |
---|
blanking+ piercing +forming Turning Notching +Dimpling Plating |
4. Process Details
Process / Operation | Notching +Dimpling |
Outsource | No |
Machine / Cell | Press Shop |
Machine / Cell No. | Machine No 9 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|
6. Inspection Method Analysis (Current)
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 5 |
7. Root Cause Analysis (Occurance)
Why 1 | Striker cap Mono m Dimn 43.6 -0.3 ID undersize up to 43.2 mm |
Why 2 | Notch Depth oversize |
Why 3 | Notch punch pressure excess |
Why 4 | Dimple punch stroke is completed but of rod (cam) stroke stroke pressure is excess. |
Why 5 | Rod (cam)punch Length more then Dimple punch |
Root Cause (Occurance) | Dimple punch & rod (cam) Length maintain. . |
Root Cause Analysis (Outflow)
Why 1 | Gauge Worn out Required 43.3 mm |
Why 2 | Observed 43.25 |
Why 3 | Worn-out |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | Gauge checking fequriency not define |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | Notching punch length excess | Deepak | 18/10/2024 | 21/10/2024 | Completed |
Outflow | Gauge correction | P D Kulkarni | 18/10/2024 | 21/10/2024 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | 100% inspection by Gauge |
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
10. Evidance of Countermeasure
Occurance (Before) |
Press shop 1141_Occurance_Before.pptx |
Occurance (After) |
Quality 1141_Occurance_After.pdf |
Outflow (Before) |
Press Shop 1141_Outflow_Before.pdf |
Outflow (After) |
Inspection 1141_Outflow_After.pdf |
11. Horizontal Deployment
Horizontal Deployment Required | No |
Applicable Machine / Model / Plant | Press shop |
12. Document Review
Documents | ControlPlan, WISOP |
Specify Other Document | WI |
13. Effectiveness Of Action
Reviewed Quantity | |
Reason for submission |