QFR No - 8000804510
Defect Details
NC No. 8000804510
NC Date 16/09/2022
NC Submission Date
Part No. 520PB00102
Part Name RAW TUBE FOR LH EXTENSION
Supplier Name & Code 101109-TUBE INVESTMENTS OF INDIA LIMI
ETL Plant 1136-ETL Suspension Sanand
Defect Details DEEP MARK-INSIDE LINE MARK
 
1. Problem Description
Defect Description Deep Line Marks in ID
Detection Stage Inprocess
Problem Severity Aesthetic
NG Quantity 8
Is Defect Repeatative? Yes
Defect Sketch / Photo zmbv35ocemqkce1uvbnl5riy.jpg
Supplier Communication Details
Quality Head Email ID anandms@tii.murugappa.com
Plant Head/CEO Email ID BhatnagarS@tii.murugappa.com
MD Email ID mukeshahuja@tii.murugappa.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
2100
0
0
1000
400
3500
Check Qty
2100
0
0
1000
400
3500
NG Qty
8
0
0
0
0
8
 
Scrap 8
Rework 0
Under Deviation 0
Containment Action
1. All available CL tubes segregation done at both ETL & TI Sanand WH and identified with blue marker inside tube ID. 2. All available Long Length tubes segregation done at TI Sanand WH and identified with blue marker inside tube ID. 3. No stock available at plant in Long length.
 
3. Process Flow
Process Flow Description
Plant Process Flow :- Slitting - Tube rolling - Annealing - Wet Process - Push Pointing/Swaging - Final drawing - Straightening - Cutting - ECT - Inspection - Packing - Dispatch to TI Sanand WH. Sanand WH Process Flow :- Inward Inspection - Storage - Cutting - Deburring - Cleaning - Inspection - Packing in Bins - Dispatch to ETL Sanand.
 
4. Process Details
Process / Operation Wet process & Tube drawing
Outsource No
Machine / Cell Draw Bench
Machine / Cell No. 40T Draw Bench
5. Problem Analysis
Type Possible Cause Fact Verification Jud
ManOperator SkillVerified through Gemba observation and found Operator Skill as per MatrixO
MaterialHollow ID mark tubeVerified through Simulation and found that ID mark generatedO
MaterialHollow tube ID wetVerified through Simulation & found the (ID Scoring mark ) defective part generated for this cause.X
ToolPlug damageVerified through Simulation and found that ID mark/scoring mark generatedO
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method Visual. (By finger)
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 5 Nos
7. Root Cause Analysis (Occurance)
Why 1 ID score mark tubes found at Customer ETL end in Cut Length.
Why 2 Plug pick up mark in drawing.
Why 3 Inside diameter of the tube wet
Why 4 Sucker side Dryer fan not working.
Why 5 Plug got pick up mark due to Wet ID.
Root Cause (Occurance) Hollow tube ID wet
 
Root Cause Analysis (Outflow)
Why 1 ID score mark tubes found at Customer ETL end in Cut Length.
Why 2 Not detected during final inspection.
Why 3 Inspection done as per sampling plan Ref. IS 4711 - 1974
Why 4 By system design
Why 5
Root Cause (Outflow) Inspection was done on sampling basis. (IS 4711 - 1974)
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceSucker side dryer fan rectifiedMr. Jadhav22/08/202221/08/2022Completed
Outflow1. 100 % Inspection will be done at both ends of the tube. (Next three Lots) 2. Sampling qty will be doubled during final inspection. (IS 4711 - 1974)Mr. Sangmesh23/09/202220/09/2022Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details 1.100 % Inspection will be done at both ends of the tube. (Next three Lots) 2. Sampling qty doubled during final inspection. (IS 4711 - 1974) 3. On draw bench during first off , 2nos & hourly Visual. (By finger)
Inspection Method Other
Other Inspection Method Visual (By finger)
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) Left side sucker Fan was not working.
253_Occurance_Before.pptx
Occurance (After) Sucker side dryer fan rectified.
253_Occurance_After.pptx
Outflow (Before) Inspection was done on sampling basis. (IS 4711 - 1974)
253_Outflow_Before.pptx
Outflow (After) 1. 100 % Inspection will be done at both ends of the tube. (Next three Lots) 2. Sampling qty will be doubled during final inspection. (IS 4711 - 1974)
253_Outflow_After.pptx
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant Applicable for all CDW tubes.
 
12. Document Review
Documents InspCheckSheet
Specify Other Document NO
 
13. Effectiveness Of Action
Reviewed Quantity 1134
Reason for submission VERFIED 1134 NOS. RAW TUBE PART FOUND OK. VERIFICATION WAS MADE FOR 5 LOTS 100%.