QFR No - 8000863226
Defect Details
NC No. 8000863226
NC Date 16/02/2024
NC Submission Date
Part No. S2JL05733B
Part Name PISTON ROD BOTH SIDE M/C _MY 18
Supplier Name & Code 101255-MAHAVIR INDUSTRIES
ETL Plant 1118-ETL E-92,93 Suspension
Defect Details DIMETER UNDERSIZE-5.5-0.1 ID IUNDER SIZE
 
1. Problem Description
Defect Description Piston rod ID 5.5-01 found Under size
Detection Stage Receipt
Problem Severity Function
NG Quantity 26
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID quality@mahavirind.co.in
Plant Head/CEO Email ID planthead@mahavirind.co.in
MD Email ID
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
4200
0
0
1200
600
6000
Check Qty
4200
0
0
1200
600
6000
NG Qty
27
0
0
3
0
30
 
Scrap 27
Rework 3
Under Deviation 0
Containment Action
All Suspected material verification at customer end
 
3. Process Flow
Process Flow Description
R/M Received- R/M Inward- band saw parting - straightening - 1st side chamfer-2nd side chamfer- 5mm Drilling-rough grinding- CNC-1st (Mounting)-CNC -2nd (Pist.side)- Cross hole Drilling- Cross Hole Chafer- IDF5.4 (1.4Cross hole) Burr Deburring - Final Inspection - Packing- Dispatch.
 
4. Process Details
Process / Operation IDF5.4 (1.4Cross hole) Burr Deburring
Outsource Yes
Machine / Cell Drilling machine-1
Machine / Cell No. Drilling Section
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MethodHard burr At Main ID5.4 Hole of Cross Hole 1.4Cross Hole Hard burr Remove by machine stop condition on Drilling Machine.O
 
6. Inspection Method Analysis (Current)
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
7. Root Cause Analysis (Occurance)
Why 1 Main ID 5.4mm under size
Why 2 Heavy burr occurred at main id During cross hole 1.4mm Drilling Process.
Why 3 Occurred Burr Remove By 5.4 Reamer as Machine standing condition.
Why 4
Why 5
Root Cause (Occurance) Occurred Burr Remove By 5.4 Reamer as Machine standing condition.
 
Root Cause Analysis (Outflow)
Why 1 Main ID 5.4mm under size
Why 2 Sampling basis ID parameters verification By PPG After burr remove process on Drilling Machine.
Why 3 Gauge Not Available on ID 5.4 Main hole ( Cross Hole) Deburring Process Stage.
Why 4
Why 5
Root Cause (Outflow) Gauge Not Available on ID 5.4 Main hole ( Cross Hole) Deburring Process Stage.
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceOccurred Burr Deburring By 5.4 Reamer as Machine Running condition.Line quality Incharge17/02/202422/02/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details 100% Main ID Inspection By New PPG on Deburring Stage.
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) Deburring Process Machine Stand Condition
680_Occurance_Before.pptx
Occurance (After) Deburring Process Machine Running Condition
680_Occurance_After.pptx
Outflow (Before) 1)Sampling Basis ID inspection .2) PPG not available on deburring machine .
680_Outflow_Before.pptx
Outflow (After) 1)100% ID Inspection On Deburring Process. 2) PPG Arrange On Deburring Machine.
680_Outflow_After.pptx
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant All Hallow Piston Rod
 
12. Document Review
Documents ControlPlan, PFMEA
Specify Other Document NO
 
13. Effectiveness Of Action
Reviewed Quantity 1200
Reason for submission no any issue observed after action taken.