QFR No - 8000873533
Defect Details
NC No. 8000873533
NC Date 06/05/2024
NC Submission Date
Part No. 550DZ04002
Part Name FORK BOLT - 5TSF
Supplier Name & Code 100189-SANGKAJ STEEL PVT LTD.
ETL Plant 1117-ETL K-228/9 Suspension
Defect Details NOT AS PER SPECIFICATION-THREAD MISSING
 
1. Problem Description
Defect Description THREAD MISSING
Detection Stage Inprocess
Problem Severity Fitment
NG Quantity 4
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID qualityassurance@sangkaj.com
Plant Head/CEO Email ID steel@sangkaj.com
MD Email ID anirudh.2007@hotmail.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
0
0
0
700
0
700
Check Qty
0
0
0
700
0
700
NG Qty
0
0
0
1
0
1
 
Scrap 1
Rework 0
Under Deviation 0
Containment Action
Sangkaj Steel End all FG Material Segregated and no NG Qty found. No material available at customer end.
 
3. Process Flow
Process Flow Description
RM Inward-RM Inspection-Traub Machining-Grinding-Milling-Deburring-Tapping-Rolling-Plating-FInal Inspection-Dispatch
 
4. Process Details
Process / Operation Thread Rolling
Outsource No
Machine / Cell Thread Rolling Machine
Machine / Cell No. 01
5. Problem Analysis
Type Possible Cause Fact Verification Jud
ManNew operatorThread Rolling done by Experienced OperatorO
MethodInadequate Inspection MethodThreads are Checked Visually OnlyX
MaterialInput Material not OKInput material having Pre-roll Diameter within Specification,O
ToolTool Wear outThread Rolls life was not Over, Resharpening done RecentlyO
MethodSetup Part Mix upoperator Setting method observed unsatisfactory, this may have lead to setup piece mix-upX
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method Visual Inspection
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
7. Root Cause Analysis (Occurance)
Why 1 Threading Washout Parts Found at Customer End
Why 2 Threads Not Completely formed during Rolling
Why 3 While Setting Full Pressure not Applied on Parts
Why 4 Setting Parts produced on Low Pressure not kept Separately and got mixed up with OK parts after Setting.
Why 5
Root Cause (Occurance) Setting Parts Mix-up
 
Root Cause Analysis (Outflow)
Why 1 Threading Washout Parts Found at Customer End
Why 2 Threads Washout parts skipped from Final Inspection
Why 3 threads are checked Visually only & in visual inspection inspector not able to arrest such parts.
Why 4 Single Inspector Need to check multiple parameters related to aesthetics` along with threading
Why 5 Inspection Method is not proper.
Root Cause (Outflow) Inspection Method is not proper.
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OutflowDuring Visual Inspection, single Inspector checks for all visual Defects Including threading, due to this by mistake defective threading Parts skips to customer End. To avoid this one more Inspector is Deputed for inspection of threading. Along with Visual Inspection 100% major Diameter Inspection with PRG will be done.MR. Anil Chaudhari13/05/202413/05/2024Completed
OccuranceOn thread Rolling Machine, Closed bins for Rejection & Rework are Provided having One way Entry. Operator will keep the Setup Parts in these bins depending on Inspection Result. As these bins are for one way entry only, reduces the chances Part Mix-up. Also Instructions given to Operator to take part for setting identified with red paint to get it recognized visually if by mistake got mixed up in ok parts.Mr. Anil Chaudhari15/05/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details 100% threading Major Dia. Inspection with Ring gauge of 25.65mm
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) During Setup, Operator Directly mix Setup Pieces in regular ok material.
786_Occurance_Before.pptx
Occurance (After) Closed Rework & Rejection bins having one way Entry are Provided on Machines. Also part taken for Setup to be identified with Red Paint to make it visually recognizable in OK parts.
786_Occurance_After.pptx
Outflow (Before) Only Visual Inspection is done for Threading
786_Outflow_Before.pptx
Outflow (After) Inspection Method is changed, 100% Inspection of major Diameter is Implemented
786_Outflow_After.pptx
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant All Fork Bolt having M26X1-6g threading
 
12. Document Review
Documents ControlPlan, WISOP, InspCheckSheet
Specify Other Document None
 
13. Effectiveness Of Action
Reviewed Quantity 150
Reason for submission OK