QFR No - 8000878522
Defect Details
NC No. 8000878522
NC Date 15/06/2024
NC Submission Date
Part No. 520HL00202
Part Name OIL LOCK COLLAR
Supplier Name & Code 101255-MAHAVIR INDUSTRIES
ETL Plant 1146-ETL Suspension Narasapura
Defect Details DIAMETER OVER SIZE-OD OVER SIZE
 
1. Problem Description
Defect Description OIL LOCK COLLAR OD MORE ISSUE
Detection Stage Inprocess
Problem Severity Fitment
NG Quantity 635
Is Defect Repeatative? Yes
Defect Sketch / Photo bhpnhqxb2aqiqeo31315nure.gif
Supplier Communication Details
Quality Head Email ID quality@mahavirind.co.in
Plant Head/CEO Email ID planthead@mahavirind.co.in
MD Email ID
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
4800
3200
0
0
0
8000
Check Qty
4800
3200
0
0
0
8000
NG Qty
635
0
0
0
0
635
 
Scrap 0
Rework 635
Under Deviation 0
Containment Action
All Suspected Material Segregation at customer End .
 
3. Process Flow
Process Flow Description
Rm Inward- store- Parting on Traub Machine - ID Chamfer - OD Grinding - Plating - Final Inspection- Dispatch
 
4. Process Details
Process / Operation OD Grinding -
Outsource No
Machine / Cell Centerless Grinding
Machine / Cell No. CLG-7
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MaterialHard MaterialHardness observed 78-84 HRBX
ToolWrong Grade Grinding Wheel UseThe control wheel and grinding wheel were of the correct grade and size.X
ManUnskilled Centerless Grinding Operator.New OperatorO
MachineMachine Condition Not OkThe control wheel slide locking screw is not properly locking.O
MethodMachining Process and Inspection Method Wrong."The OD grinding process method and inspection method are acceptableX
 
6. Inspection Method Analysis (Current)
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
7. Root Cause Analysis (Occurance)
Why 1 DIAMETER OVER SIZE-OD OVER SIZE
Why 2 After dressing the control wheel, the operator did not properly tighten the slide
Why 3 The control wheel slide locking screw thread is worn.
Why 4 The operator is not aware of the side effects of the sliding locking screw
Why 5 New operator.
Root Cause (Occurance) The control wheel slide locking screw thread is worn.
 
Root Cause Analysis (Outflow)
Why 1 DIAMETER OVER SIZE-OD OVER SIZE
Why 2 Defected parts Not Detect On Final inspection Stage.
Why 3 New Final Inspector
Why 4
Why 5
Root Cause (Outflow) New Final Inspector
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceCenterless Grinding Machine maintenance was done as per the PM scheduleProduction And maintenance head18/06/202418/06/2024Completed
OutflowTraining for the operator and work instructions are displayed on the CLG machine.Quality Head19/06/202419/06/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details An additional snap gauge is provided on the CLG grinding machine.
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) The control wheel slide locking screw thread is worn.
872_Occurance_Before.docx
Occurance (After) Centerless Grinding Machine maintenance was done as per the PM schedule
872_Occurance_After.docx
Outflow (Before) New Final Inspector r
872_Outflow_Before.docx
Outflow (After) Training for the operator and work instructions are displayed on the CLG machine.
872_Outflow_After.docx
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant All Oil Lock Collar
 
12. Document Review
Documents ControlPlan, PFMEA, WISOP
Specify Other Document OJT
 
13. Effectiveness Of Action
Reviewed Quantity 5000
Reason for submission Reviewed next two lots found ok