QFR No - 8000895939
Defect Details
NC No. | 8000895939 |
NC Date | 17/10/2024 |
NC Submission Date | |
Part No. | F2DZ04603B |
Part Name | FORK BOLT J1A & J1D |
Supplier Name & Code | 100189-SANGKAJ STEEL PVT LTD. |
ETL Plant | 1117-ETL K-228/9 Suspension |
Defect Details | NOT AS PER SPECIFICATION-GROOVE WITH UNDER SIZE |
1. Problem Description
Defect Description | Groove width undersize Specification: 4.5 +0.2 Observation: 2.88 |
Detection Stage | Inprocess |
Problem Severity | Fitment |
NG Quantity | 1 |
Is Defect Repeatative? | No |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | qualityassurance@sangkaj.com |
Plant Head/CEO Email ID | steel@sangkaj.com |
MD Email ID | anirudh.2007@hotmail.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
288
|
0
|
0
|
550
|
300
|
1138
|
Check Qty |
288
|
0
|
0
|
550
|
300
|
1138
|
NG Qty |
0
|
0
|
0
|
0
|
0
|
0
|
Scrap | 0 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
All the Material at Endurance & at sangkaj steel checked and no NG part Found |
3. Process Flow
Process Flow Description |
---|
RM Inward and inward Inspection-Wire Drawing-Straightening-Bar Parting-CNC 1st- CNC2nd-Milling-Tapping-plating-Final Inspection-Packing & Dispatch |
4. Process Details
Process / Operation | CNC turning 2nd |
Outsource | Yes |
Machine / Cell | CNC Machine |
Machine / Cell No. | 2 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Tool | Insert Broken | Defective piece observed with groove width undersize by1.62mm, which occures only after insert break | X |
Man | New operator | Regular and Experienced operator Dployed for Production. | O |
Material | Input Material Not OK | Cut Blanks found ok as all the blanks are cut through same bar. | O |
Machine | Variation due to machine | Variation due to Machine not Causes dimension undersize by 1.62mm | O |
Method | Less Sampling Size | Groove width is checked with width gauge on Sampling basis. | X |
6. Inspection Method Analysis (Current)
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 10:100 |
7. Root Cause Analysis (Occurance)
Why 1 | Groove Width Undersize Part Found at Customer End |
Why 2 | Incomplete Operation is done during Grooving. |
Why 3 | Insert Broken before the Set Tool Life. |
Why 4 | |
Why 5 | |
Root Cause (Occurance) | Insert Broken before the Set Tool Life. |
Root Cause Analysis (Outflow)
Why 1 | Groove Width Undersize Part Found at Customer End |
Why 2 | Defective Parts Skipped from the Final Inspection |
Why 3 | Part Checked on Sampling basis with slip type width gauge. |
Why 4 | Less Sampling Size |
Why 5 | |
Root Cause (Outflow) | Less Sampling Size during Final Inspection. |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | Revalidation of Insert Life is done by varying the Process Parameters. Previous set Life was 800 No`s Per Side. By Setting the Process Parameters at extreme limit of their Specification, the new Insert Life set is 700 No`s. | Mr. Santosh Raut | 22/10/2024 | 22/10/2024 | Completed |
Outflow | Inspection method Changed. 100% Inspection of Groove with Slip type Width Gauge is done During the Final Inspection. | Mr. A.A. Joshi | 22/10/2024 | 22/10/2024 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | 100% inspection of Groove with Slip type WIdth Gauge. |
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
10. Evidance of Countermeasure
Occurance (Before) |
Tool Life-800 Nos 1157_Occurance_Before.pptx |
Occurance (After) |
Tool Life -700 Nos 1157_Occurance_After.pptx |
Outflow (Before) |
Inspection on Sampling Basis 1157_Outflow_Before.pptx |
Outflow (After) |
100% Inspection with Width gauge 1157_Outflow_After.pptx |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | Fork Bolt AABM |
12. Document Review
Documents | ControlPlan, InspCheckSheet |
Specify Other Document | No Other |
13. Effectiveness Of Action
Reviewed Quantity | 50 |
Reason for submission | Interlocking required for tool breakage |