QFR No - 8000902882
Defect Details
NC No. | 8000902882 |
NC Date | 09/12/2024 |
NC Submission Date | |
Part No. | F2PA00202B |
Part Name | BOTTOM CASE RING RE J1A |
Supplier Name & Code | 100990-JAIRAJ ANCILLARIES PVT LTD |
ETL Plant | 1117-ETL K-228/9 Suspension |
Defect Details | NOT AS PER SPECIFICATION-BREAK |
1. Problem Description
Defect Description | BREAK |
Detection Stage | Receipt |
Problem Severity | Function |
NG Quantity | 700 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo | 3tkupsqk0tnofazl2odnzfet.jpg |
Supplier Communication Details
Quality Head Email ID | planthead.aurangabad@jairajgroup.com |
Plant Head/CEO Email ID | vp@jairajgroup.com |
MD Email ID | rajiv@jairajgroup.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
5000
|
0
|
0
|
2000
|
0
|
7000
|
Check Qty |
5000
|
0
|
0
|
2000
|
0
|
7000
|
NG Qty |
700
|
0
|
0
|
0
|
0
|
700
|
Scrap | 700 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
All available material checked 100 % at ETL end and found 700 no. defective out of 5000 no. checked. All available inhouse FG material checked 100% and found no defective parts out of 2000 no. checked. |
3. Process Flow
Process Flow Description |
---|
Injection Moulding & Annealing |
4. Process Details
Process / Operation | Injection Moulding & Annealing |
Outsource | No |
Machine / Cell | IMM-09 |
Machine / Cell No. | IMM-09 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Man | Man Power does not aware about this defect . | Verifed that operator , In process inspector & Final Inspector aware about this defect . | O |
Material | RM Grade not as per CP . | Check with MTC & found ok as per specification | O |
Machine | OCS & control plan not followed by Machine Operator . | Verified as per Cp & OCS found ok | O |
Method | Annealing surface volume in tank in sufficient to dip the parts in medium. | Verified and found due to small tank top parts are getting float in medium . | X |
Method | RM preheating not done | Verified as per CP & OCS found ok , As per Standard Specification | O |
Machine | Barrel Temp High / Low | Verified as per Cp & OCS found ok , As per Standard Specification | O |
Tool | Air trapped & air vent inefficient open | Verified the air vent and found ok | O |
6. Inspection Method Analysis (Current)
Inspection Method | Other |
Other Inspection Method | Visually |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 5 |
7. Root Cause Analysis (Occurance)
Why 1 | Parts are getting broken erratically on weld line surface. |
Why 2 | Parts are not getting fully dipped in annealing medium |
Why 3 | Due to parts are getting floated above the medium surface |
Why 4 | Due to Annealing tank size small , parts surface not completely annealed. |
Why 5 | |
Root Cause (Occurance) | Due to Annealing tank size small , top parts surface not completely annealed resulting into insufficient annealing . Due to Annealing tank size small , parts surface not completely annealed resulting in breakages erratically. |
Root Cause Analysis (Outflow)
Why 1 | Parts are getting broken erratically on weld Line surface. |
Why 2 | Parts are getting skipped from Operator and Final Inspector |
Why 3 | After annealing process , parts are getting checked on sampling Inspection |
Why 4 | Lack of awareness of highlighted defect. |
Why 5 | |
Root Cause (Outflow) | Lack of awareness of highlighted defect. |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | Big Annealing tank to Incorporate so that max parts are getting covered in one annealing cycle. | Ganesh Mhaske | 18/12/2024 | 18/12/2024 | Completed |
Occurance | Annealing record Register monitoring started | Ganesh mhaske | 18/12/2024 | 18/12/2024 | Completed |
Outflow | Awareness training given to in process inspector & Final Inspector about highlighted defect . | Amol Chidre | 20/12/2024 | 20/12/2024 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | 100% Visual Inspection for part softness after annealing. |
Inspection Method | Other |
Other Inspection Method | Visually |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
10. Evidance of Countermeasure
Occurance (Before) |
Earlier small Annealing tank does not cover part max occupancy per cycle . Parts are getting open in medium due to floating on
surface at top side which may be the probable cause 1264_Occurance_Before.pptx |
Occurance (After) |
Now Big Size Annealing tank implemented so that max parts are covered per cycle. Annealing Monitoring record started. 1264_Occurance_After.pdf |
Outflow (Before) |
Earlier Parts Softness & ductility after annealing process was checked at sampling basis. 1264_Outflow_Before.pdf |
Outflow (After) |
Parts softness and Ductility checking with 100% Inspection with OJT to In process and Firewall Inspectors 1264_Outflow_After.pdf |
11. Horizontal Deployment
Horizontal Deployment Required | No |
Applicable Machine / Model / Plant | N/A |
12. Document Review
Documents | WISOP, InspCheckSheet |
Specify Other Document | N/A |
13. Effectiveness Of Action
Reviewed Quantity | 100 |
Reason for submission | ok |