QFR No - 7000932465
Defect Details
NC No. 7000932465
NC Date 26/07/2023
NC Submission Date
Part No. 550BZ01402
Part Name CAP OIL LOCK - DF01
Supplier Name & Code 100106-SHARP ENGINEERS.
ETL Plant 1136-ETL Suspension Sanand
Defect Details PARALITY NOT OK.-Parallelism out of specification 0.04 mm
 
1. Problem Description
Defect Description Parallelism NG of cap oil lock
Detection Stage Receipt
Problem Severity Function
NG Quantity 2445
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID quality@apw3.co.in
Plant Head/CEO Email ID kurund.ma@sharp-engineers.com
MD Email ID urkhandelwal@sharp-engineers.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
22000
20000
0
10000
0
52000
Check Qty
22000
20000
0
10000
0
52000
NG Qty
2445
0
0
6
0
2451
 
Scrap 0
Rework 2445
Under Deviation 0
Containment Action
Segregation done immediately for suspected material and defective 2445 nos rejected and quarantine from ok parts,
 
3. Process Flow
Process Flow Description
10) RM Inward inspection 20) Storage 30) Parting, Drilling & Forming 40) Chamfering 50) OD Ø 18.05 grinding 60) Plating Process (Outsource) 70) Inward Inspection 80)
 
4. Process Details
Process / Operation Parting, Drilling & Forming
Outsource No
Machine / Cell TRAUB MACHINE
Machine / Cell No. SE/SSAL/01
5. Problem Analysis
Type Possible Cause Fact Verification Jud
ManUn-skilled OperatorStage wise skill matrix and operator license are evident as per F/HR/06O
MachineInadequate check Point in JH check sheetMonthly JH check sheet available on machine and all the check point is being checked and recorded asO
MethodImproper Material FlowMaterial flow defined as per process flow and control plan and being followedO
ToolTool life not getting as definedTool life is defined. But tool is found wear out before defined frequency.X
MaterialIncorrect Raw MaterialMaterial observed as per customer requirement Ø16.10 EN1A , MTC verified as per drawing specificatioO
 
6. Inspection Method Analysis (Current)
Inspection Method Sp. Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 1:1
7. Root Cause Analysis (Occurance)
Why 1 Tool worn out on 500/sharpening earlier than defined frequency , drill worn out sometimes at end of the tool life near @500 Nos.
Why 2 In SS drill variation observed for parallelism at end of the tool life 500/sharpening.
Why 3
Why 4 Drill life not getting as per defined frequency .
Why 5
Root Cause (Occurance) CAP OIL LOCK (df) tool life defined for 500/sharpening but drill Ø14.10 worn out earlier than defined frequency. Dimensional variation found at end of the tool life after 500/sharpening.
 
Root Cause Analysis (Outflow)
Why 1 Excess parallelism not detected at final inspection
Why 2 Sampling basis inspection as per SSPN 32:1200 Nos.
Why 3 Sampling frequency defined by system as per control plan.
Why 4
Why 5
Root Cause (Outflow) 100% inspection is not being done for parallelism.
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OutflowFor TIN Coated Drill Initially 100% inspection will be done for parallelism to monitoring the results, after sustenance verification and joint discussion with ETL & SHARP inspection frequency will be changed .Mr.Shaikh L.N.26/07/202327/07/2023Completed
OccuranceSS Tool life not getting as per defined so view of improvement in tool life inplace of SS TIN (Titanium Nitride ) coated drill is being used, SPC done for coated and non coated drill after process validation TIN coated drill defined and added in the control plan.Mr. DattaPandhre27/07/202327/07/2023Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details For TIN Coated Drill Initially 100% inspection will be done for parallelism to monitoring the results, after sustenance verification and joint discussion with ETL & SHARP inspection frequency will be changed .
Inspection Method Sp. Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 1:1
10. Evidance of Countermeasure
Occurance (Before) CAP OIL LOCK (df) tool life defined for 500/sharpening but drill Ø14.10 worn out earlier than defined frequency. Dimensional variation found at end of the tool life after 500/sharpening.
511_Occurance_Before.pptx
Occurance (After) SS Tool life not getting as per defined so view of improvement in tool life in place of SS TIN (Titanium Nitride) coated drill is being used, SPC done for coated and non coated drill after process validation TIN coated drill defined and added in the control plan. Tool life defined 600/sharpening.
511_Occurance_After.pptx
Outflow (Before) 100% inspection is not being done for parallelism.
511_Outflow_Before.pptx
Outflow (After) For TIN Coated Drill Initially 100% inspection will be done for parallelism to monitoring the results, after sustenance verification and joint discussion with ETL & SHARP inspection frequency will be changed .
511_Outflow_After.pptx
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant HMSI(K86/K0LA)
 
12. Document Review
Documents ControlPlan, PFMEA, WISOP, ProcessFlowChart, InspCheckSheet
Specify Other Document NA
 
13. Effectiveness Of Action
Reviewed Quantity
Reason for submission