QFR No - 8000868408
Defect Details
NC No. | 8000868408 |
NC Date | 22/03/2024 |
NC Submission Date | |
Part No. | F2BZ05712B |
Part Name | CAP OIL LOCK - J1D FF (10mm taper) |
Supplier Name & Code | 101255-MAHAVIR INDUSTRIES |
ETL Plant | 1117-ETL K-228/9 Suspension |
Defect Details | NOT AS PER SPECIFICATION-PARELLELISM MORE |
1. Problem Description
Defect Description | Parallelism more |
Detection Stage | Inprocess |
Problem Severity | Function |
NG Quantity | 42 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | quality@mahavirind.co.in |
Plant Head/CEO Email ID | planthead@mahavirind.co.in |
MD Email ID |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
3500
|
0
|
0
|
1750
|
0
|
5250
|
Check Qty |
3500
|
0
|
0
|
1750
|
0
|
5250
|
NG Qty |
42
|
0
|
0
|
5
|
0
|
47
|
Scrap | 47 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
All suspected FG Material Segregation at customer end and Final Inspection Area . |
3. Process Flow
Process Flow Description |
---|
Raw material Inward - Raw Material store -Parting on Traub machine -Bottom side ID(10.5)chamfer-OD Grinding -Semi Finish Inward - CNC ID Boring, Taper (10°)Turing, Facing -Plating Green)- Final inspection- Packing- Dispatch . |
4. Process Details
Process / Operation | Parting on Traub machine -Face uneven |
Outsource | Yes |
Machine / Cell | Traub(A-25)-02 |
Machine / Cell No. | Traub Section |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Machine | Parting on Traub machine -Face uneven | Bottom side Ring Chatter marks | X |
6. Inspection Method Analysis (Current)
Inspection Method | Instrument |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 20pc/Bin |
7. Root Cause Analysis (Occurance)
Why 1 | Parallelism More |
Why 2 | Chatter marks On bottom side |
Why 3 | Bottom Side Face Operation Finish On Traub Machine. |
Why 4 | |
Why 5 | |
Root Cause (Occurance) | Bottom Side Face Operation Finish On Traub Machine |
Root Cause Analysis (Outflow)
Why 1 | Parallelism More |
Why 2 | Parallelism Not 100% Inspection after CNC Machining |
Why 3 | Dial Test Indicator Instrument Not Available on CNC machine. |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | Dial Test Indicator Instrument Not Available on CNC machine. |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Outflow | Dial Test Indicator Instrument Arrange on CNC machine. | quality Head | 24/03/2024 | 24/03/2024 | Completed |
Outflow | Work Instruction Display on Defected Material Handling | Quality Head | 22/04/2024 | 22/03/2024 | Completed |
Occurance | Process add of Bottom facing on CNC Machine | Quality Head | 22/03/2024 | 22/03/2024 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | 100% Parallelism Parameter Check On CNC machine |
Inspection Method | Instrument |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
10. Evidance of Countermeasure
Occurance (Before) |
Parting ,bottom Side Chamfer (0.8x45°) and Facing Process on Traub Machine. 721_Occurance_Before.pptx |
Occurance (After) |
CNC Process add-Chamfer(0.8X45°) and bottom side facing process. After Traub Parting. 721_Occurance_After.pptx |
Outflow (Before) |
Sample Basis (10-15Nos/Hr) Parallelism Verification On CNC Machine. 721_Outflow_Before.pptx |
Outflow (After) |
1)Parallelism parameter 100% Verification By Comparator Stand On CNC Machine. 2) OJT For Comparator Handling to CNC Operator 721_Outflow_After.pptx |
11. Horizontal Deployment
Horizontal Deployment Required | No |
Applicable Machine / Model / Plant | Only For Cap oil lock J1D Model |
12. Document Review
Documents | ControlPlan, PFMEA, WISOP, ProcessFlowChart |
Specify Other Document | no |
13. Effectiveness Of Action
Reviewed Quantity | 180 |
Reason for submission | OK |